HL incident on 2011-04-10 — IL

Operator
Bp West Coast Products L.l.c.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,500
Incident datetime
2011-04-10 16:45
Report number
Location
IL
Narrative
04/10/2011, bp la basin experienced an approximate 25.2 gallon release of crude oil to the primary containment area of vault 17 located in an auto storage yard approximately one mile west of terminal 2. While responding to a call from the operations control center (occ), two bp la basin operations employees observed oil leaking onto the vault floor from the packing of mov 2439. Approximately 2' of product was observed at the bottom of the vault. Pressure in mov 2439 and associated lines was relieved and both the mov and associated lines were isolated. Investigation: following findings and observations were performed during the investigation: mov 2439 is a 24' 150# API 6d adamson chronister pipeline slab-gate valve. Following the incident this valve was transported offsite for disassembly and investigation by facility engineering personnel. The valve showed no signs of damage warranting a packing leak in its current state. The packing was inspected in september 2010 prior to the incident. The valve stem, packing box and yolk showed no signs of abnormal wear or damage. The packing failed causing a loss of primary containment due to normal wear and tear. Conclusion mov 2439 packing failure is a result of normal wear and tear. No further investigation required.
Detailed record list
Report Received Date
2011-05-09 00:00:00
Iyear
2011
Report Number
20110134
Supplemental Number
16368
Report Type
Supplemental Final
Operator Id
Name
Bp West Coast Products L.l.c.
Operator Street Address
150 West Warrenville Road
Operator City Name
Naperville
Operator State Abbreviation
IL
Operator Postal Code
60563
Local Datetime
2011-04-10 16:45:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.6
Intentional Release Bbls
0
Recovered Bbls
0.6
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2011-04-10 16:45:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
On Site Datetime
2011-04-10 16:50:00
Nrc Rpt Datetime
2011-04-10 18:45:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Line 82d
Segment Name
Csfm 1198
Onshore State Abbreviation
Ca
Onshore Postal Code
90802
Onshore City Name
Long Beach
Onshore County Name
Los Angeles County
Designated Location
Milepost/valve Station
Designated Name
Vault 17
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Mainline
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
100
Est Cost Prop Damage
1500
Est Cost Emergency
3000
Est Cost Environmental
0
Est Cost Other
0
Prpty
4600
Pipeline Function
< 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Preparer Name
S****** D* C*****
Preparer Title
Environmental Coordinator
Preparer Email
S*************@b*.com
Preparer Telephone
5627282265
Preparer Fax
5627282760
Prepared Date
2012-01-26 00:00:00
Authorizer Name
R** K*******
Authorizer Telephone
6305362549
Authorizer Title
Dot Team Lead
Authorizer Email
K*******@b*.com
Narrative
04/10/2011, bp la basin experienced an approximate 25.2 gallon release of crude oil to the primary containment area of vault 17 located in an auto storage yard approximately one mile west of terminal 2. While responding to a call from the operations control center (occ), two bp la basin operations employees observed oil leaking onto the vault floor from the packing of mov 2439. Approximately 2' of product was observed at the bottom of the vault. Pressure in mov 2439 and associated lines was relieved and both the mov and associated lines were isolated. Investigation: following findings and observations were performed during the investigation: mov 2439 is a 24' 150# API 6d adamson chronister pipeline slab-gate valve. Following the incident this valve was transported offsite for disassembly and investigation by facility engineering personnel. The valve showed no signs of damage warranting a packing leak in its current state. The packing was inspected in september 2010 prior to the incident. The valve stem, packing box and yolk showed no signs of abnormal wear or damage. The packing failed causing a loss of primary containment due to normal wear and tear. Conclusion mov 2439 packing failure is a result of normal wear and tear. No further investigation required.
Report Received Date 2011-05-09 00:00:00
Iyear 2011
Report Number 20110134
Supplemental Number 16368
Report Type Supplemental Final
Operator Id 31610 PHMSA Enforcement
Name Bp West Coast Products L.l.c.
Operator Street Address 150 West Warrenville Road
Operator City Name Naperville
Operator State Abbreviation IL
Operator Postal Code 60563
Local Datetime 2011-04-10 16:45:00
Location Latitude 33.78114 Google Maps OpenStreetMap
Location Longitude -118.22177 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.6
Intentional Release Bbls 0
Recovered Bbls 0.6
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2011-04-10 16:45:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
On Site Datetime 2011-04-10 16:50:00
Nrc Rpt Datetime 2011-04-10 18:45:00
Nrc Rpt Num 972546 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Line 82d
Segment Name Csfm 1198
Onshore State Abbreviation Ca
Onshore Postal Code 90802
Onshore City Name Long Beach
Onshore County Name Los Angeles County
Designated Location Milepost/valve Station
Designated Name Vault 17
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Mainline
Release Type Leak
Leak Type Seal Or Packing
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 100
Est Cost Prop Damage 1500
Est Cost Emergency 3000
Est Cost Environmental 0
Est Cost Other 0
Prpty 4600
Pipeline Function < 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Preparer Name S****** D* C*****
Preparer Title Environmental Coordinator
Preparer Email S*************@b*.com
Preparer Telephone 5627282265
Preparer Fax 5627282760
Prepared Date 2012-01-26 00:00:00
Authorizer Name R** K*******
Authorizer Telephone 6305362549
Authorizer Title Dot Team Lead
Authorizer Email K*******@b*.com
Narrative 04/10/2011, bp la basin experienced an approximate 25.2 gallon release of crude oil to the primary containment area of vault 17 located in an auto storage yard approximately one mile west of terminal 2. While responding to a call from the operations control center (occ), two bp la basin operations employees observed oil leaking onto the vault floor from the packing of mov 2439. Approximately 2' of product was observed at the bottom of the vault. Pressure in mov 2439 and associated lines was relieved and both the mov and associated lines were isolated. Investigation: following findings and observations were performed during the investigation: mov 2439 is a 24' 150# API 6d adamson chronister pipeline slab-gate valve. Following the incident this valve was transported offsite for disassembly and investigation by facility engineering personnel. The valve showed no signs of damage warranting a packing leak in its current state. The packing was inspected in september 2010 prior to the incident. The valve stem, packing box and yolk showed no signs of abnormal wear or damage. The packing failed causing a loss of primary containment due to normal wear and tear. Conclusion mov 2439 packing failure is a result of normal wear and tear. No further investigation required.

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