HL incident on 2011-04-04 — TX

Operator
Enbridge Energy, Limited Partnership
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$67,647
Incident datetime
2011-04-04 08:00
Report number
Location
TX
Narrative
On monday, april 4, 2011 superior terminal and plm personnel began investigating a show of oil near valve 221-v-sp1 which is located in the road ditch outside the se corner of the tank 8 berm. At the time of the discovery the volume and expected costs to manage the leak was anticipated to be less than $50,000. On april 8 it was determined that to fully investigate and remediate the cause of the leak, and specifically due to the constraints associated with excavation area (sheet pilling was necessary to make the area safe for further investigation), it was very likely that the $50,000 reportability threshold would be exceeded, and therefore the nrc was notified at this time. After further investigation, a pencil sized corrosion hole was discovered at the 6 o'clock position of the pipe. The pipe was temporarily repaired with a plidco split + sleeve and the permanent repair will be a pipe replacement which is scheduled for end of q2 2011. This replacement section of pipe will be redesigned to eliminate the "dead leg" area where the leak occurred.
Detailed record list
Report Received Date
2011-05-03 00:00:00
Iyear
2011
Report Number
20110130
Supplemental Number
18545
Report Type
Supplemental Final
Operator Id
Name
Enbridge Energy, Limited Partnership
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2011-04-04 08:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.29
Intentional Release Bbls
0
Recovered Bbls
0.29
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2011-04-04 08:00:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Active Leak Was Not Suspected At This Time
On Site Datetime
2011-04-04 08:00:00
Nrc Rpt Datetime
2011-04-08 13:51:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Superior Terminal
Segment Name
Line 1 Facility Piping
Onshore State Abbreviation
Wi
Onshore Postal Code
54880
Onshore City Name
Superior
Onshore County Name
Douglas
Designated Location
Survey Station No.
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
60
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
18
Pipe Wall Thickness
0.281
Pipe Smys
42000
Pipe Specification
Api 5l X42
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
A O Smith
Pipe Coating Type
Coal Tar
Installation Year
1950
Manufactured Year
1950
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
67647
Est Cost Emergency
47000
Est Cost Environmental
8000
Est Cost Other
0
Prpty
122647
Accident Psig
25
Mop Psig
262
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Cause of leak was corrosion related.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
General Corrosion
Int Microbiological Ind
Yes
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
S**** S****
Preparer Title
Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
218-464-5754
Preparer Fax
218-464-5992
Prepared Date
2013-09-12 00:00:00
Authorizer Name
D**** S*******
Authorizer Telephone
218-464-5751
Authorizer Title
Manager Pipeline Compliance
Authorizer Email
D*************@e*******.com
Narrative
On monday, april 4, 2011 superior terminal and plm personnel began investigating a show of oil near valve 221-v-sp1 which is located in the road ditch outside the se corner of the tank 8 berm. At the time of the discovery the volume and expected costs to manage the leak was anticipated to be less than $50,000. On april 8 it was determined that to fully investigate and remediate the cause of the leak, and specifically due to the constraints associated with excavation area (sheet pilling was necessary to make the area safe for further investigation), it was very likely that the $50,000 reportability threshold would be exceeded, and therefore the nrc was notified at this time. After further investigation, a pencil sized corrosion hole was discovered at the 6 o'clock position of the pipe. The pipe was temporarily repaired with a plidco split + sleeve and the permanent repair will be a pipe replacement which is scheduled for end of q2 2011. This replacement section of pipe will be redesigned to eliminate the "dead leg" area where the leak occurred.
Report Received Date 2011-05-03 00:00:00
Iyear 2011
Report Number 20110130
Supplemental Number 18545
Report Type Supplemental Final
Operator Id 11169 PHMSA Enforcement
Name Enbridge Energy, Limited Partnership
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2011-04-04 08:00:00
Location Latitude 46.68889 Google Maps OpenStreetMap
Location Longitude -92.05972 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.29
Intentional Release Bbls 0
Recovered Bbls 0.29
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2011-04-04 08:00:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Active Leak Was Not Suspected At This Time
On Site Datetime 2011-04-04 08:00:00
Nrc Rpt Datetime 2011-04-08 13:51:00
Nrc Rpt Num 972372 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Superior Terminal
Segment Name Line 1 Facility Piping
Onshore State Abbreviation Wi
Onshore Postal Code 54880
Onshore City Name Superior
Onshore County Name Douglas
Designated Location Survey Station No.
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 60
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 18
Pipe Wall Thickness 0.281
Pipe Smys 42000
Pipe Specification Api 5l X42
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer A O Smith
Pipe Coating Type Coal Tar
Installation Year 1950
Manufactured Year 1950
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 67647
Est Cost Emergency 47000
Est Cost Environmental 8000
Est Cost Other 0
Prpty 122647
Accident Psig 25
Mop Psig 262
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Cause of leak was corrosion related.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results General Corrosion
Int Microbiological Ind Yes
Int Field Exam Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name S**** S****
Preparer Title Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 218-464-5754
Preparer Fax 218-464-5992
Prepared Date 2013-09-12 00:00:00
Authorizer Name D**** S*******
Authorizer Telephone 218-464-5751
Authorizer Title Manager Pipeline Compliance
Authorizer Email D*************@e*******.com
Narrative On monday, april 4, 2011 superior terminal and plm personnel began investigating a show of oil near valve 221-v-sp1 which is located in the road ditch outside the se corner of the tank 8 berm. At the time of the discovery the volume and expected costs to manage the leak was anticipated to be less than $50,000. On april 8 it was determined that to fully investigate and remediate the cause of the leak, and specifically due to the constraints associated with excavation area (sheet pilling was necessary to make the area safe for further investigation), it was very likely that the $50,000 reportability threshold would be exceeded, and therefore the nrc was notified at this time. After further investigation, a pencil sized corrosion hole was discovered at the 6 o'clock position of the pipe. The pipe was temporarily repaired with a plidco split + sleeve and the permanent repair will be a pipe replacement which is scheduled for end of q2 2011. This replacement section of pipe will be redesigned to eliminate the "dead leg" area where the leak occurred.

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