HL incident on 2011-04-07 — GA

Operator
Colonial Pipeline Co
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$392
Incident datetime
2011-04-07 00:31
Report number
Location
GA
Narrative
On april 7, 2011 at 00:31 et an operator discovered product around the line 32 control valve inside the dorsey facility. The line was not operating at the time and was immediately depressurized. Notifications were made to the lead operator at 00:31, the environmental specialist at 00:59, and the operations manager at 00:38. A call was placed to the state at 02:33. The area was continuously monitored while dirt and gravel were removed from around the control valve. Further examination revealed the source of the leak to be a stem seal failure in the control valve. Seal was replaced during business hours 4/7/11.
Detailed record list
Report Received Date
2011-04-27 00:00:00
Iyear
2011
Report Number
20110128
Supplemental Number
18401
Report Type
Supplemental Final
Operator Id
Name
Colonial Pipeline Co
Operator Street Address
1185 Sanctuary Parkway, Suite 100
Operator City Name
Alpharetta
Operator State Abbreviation
GA
Operator Postal Code
30009-4765
Local Datetime
2011-04-07 00:31:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.19
Intentional Release Bbls
0
Recovered Bbls
0.19
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Ignite Ind
No
Explode Ind
No
Pipe Fac Name
Dorsey Junction
Segment Name
Line 32 Pump Station
Onshore State Abbreviation
Md
Onshore Postal Code
21797
Onshore City Name
Woodbine
Onshore County Name
Carroll
Designated Location
Milepost/valve Station
Designated Name
Control Valve
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
30
Est Cost Prop Damage
392
Est Cost Emergency
2170
Est Cost Environmental
0
Est Cost Other
0
Prpty
2592
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Eq Failure Type
Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Preparer Name
A* M*******
Preparer Title
Regulatory Manager
Preparer Email
A******@c******.com
Preparer Telephone
6787622872
Preparer Fax
6787622465
Prepared Date
2013-08-06 00:00:00
Authorizer Name
A* M* T*****
Authorizer Telephone
6787622872
Authorizer Title
Regulatory Manager
Authorizer Email
A******@c******.com
Narrative
On april 7, 2011 at 00:31 et an operator discovered product around the line 32 control valve inside the dorsey facility. The line was not operating at the time and was immediately depressurized. Notifications were made to the lead operator at 00:31, the environmental specialist at 00:59, and the operations manager at 00:38. A call was placed to the state at 02:33. The area was continuously monitored while dirt and gravel were removed from around the control valve. Further examination revealed the source of the leak to be a stem seal failure in the control valve. Seal was replaced during business hours 4/7/11.
Report Received Date 2011-04-27 00:00:00
Iyear 2011
Report Number 20110128
Supplemental Number 18401
Report Type Supplemental Final
Operator Id 2552 PHMSA Enforcement
Name Colonial Pipeline Co
Operator Street Address 1185 Sanctuary Parkway, Suite 100
Operator City Name Alpharetta
Operator State Abbreviation GA
Operator Postal Code 30009-4765
Local Datetime 2011-04-07 00:31:00
Location Latitude 39.36101 Google Maps OpenStreetMap
Location Longitude -77.03759 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.19
Intentional Release Bbls 0
Recovered Bbls 0.19
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Ignite Ind No
Explode Ind No
Pipe Fac Name Dorsey Junction
Segment Name Line 32 Pump Station
Onshore State Abbreviation Md
Onshore Postal Code 21797
Onshore City Name Woodbine
Onshore County Name Carroll
Designated Location Milepost/valve Station
Designated Name Control Valve
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Release Type Leak
Leak Type Seal Or Packing
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 30
Est Cost Prop Damage 392
Est Cost Emergency 2170
Est Cost Environmental 0
Est Cost Other 0
Prpty 2592
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Eq Failure Type Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Preparer Name A* M*******
Preparer Title Regulatory Manager
Preparer Email A******@c******.com
Preparer Telephone 6787622872
Preparer Fax 6787622465
Prepared Date 2013-08-06 00:00:00
Authorizer Name A* M* T*****
Authorizer Telephone 6787622872
Authorizer Title Regulatory Manager
Authorizer Email A******@c******.com
Narrative On april 7, 2011 at 00:31 et an operator discovered product around the line 32 control valve inside the dorsey facility. The line was not operating at the time and was immediately depressurized. Notifications were made to the lead operator at 00:31, the environmental specialist at 00:59, and the operations manager at 00:38. A call was placed to the state at 02:33. The area was continuously monitored while dirt and gravel were removed from around the control valve. Further examination revealed the source of the leak to be a stem seal failure in the control valve. Seal was replaced during business hours 4/7/11.

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