Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2011-03-22 — TX
Operator
Mustang Pipe Line Partners
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$0
Incident datetime
2011-03-22 09:58
Report number
Location
TX
Narrative
Exxonmobil personnel were on site when the incident occurred. There was a small crude stain on the soil inside the station yard. Upon excavation to check the stain, a couple of flange bolts were found loose and there was a gasket seep. The flanged bolts were torque tight, pipe section pressured up and visually inspected for any leaks. The pipeline was already down when incident occurred. Supplemental revised on 12-22-11 to correct gps coordinates in part a, removed state and county on part b, and changed g8 to g 6 equipment failure sub cause non- threaded connection failure as discussed with brian pierzina supplemental created to close the 7001 report as final. 8-22-12 7-31-13 supplemental report PHMSA requested supplemental be created to added part e 5 f data ie, ( function of pipeline system) be added to form.
Detailed record list
Report Received Date
2011-04-20 00:00:00
Iyear
2011
Report Number
20110122
Supplemental Number
18372
Report Type
Supplemental Final
Operator Id
31166
Name
Mustang Pipe Line Partners
Operator Street Address
22777 Springwoods Village Parkway E2.2b-Emp
Operator City Name
Spring
Operator State Abbreviation
TX
Operator Postal Code
77389
Local Datetime
2011-03-22 09:57:00
Location Latitude
40.5161701
Location Longitude
-88.3192648
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.5
Intentional Release Bbls
0
Recovered Bbls
0.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2011-03-22 09:58:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Pipeline Was Already Down When Incident Occured And Personnel Were On Site
On Site Datetime
2011-03-22 09:58:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Gibson City Pump Station, Ford County, Ill
Segment Name
Mustang System 18" Pipeline, Gibson City Station
Onshore State Abbreviation
Il
Onshore Postal Code
60936
Onshore City Name
Gibson City
Onshore County Name
Ford
Designated Location
Milepost/valve Station
Designated Name
Pump Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Pipe Facility Type
Interstate
Item Involved
Flange Assembly
Release Type
Leak
Leak Type
Other
Leak Type Other
Flange Bolt Needed Tightened.
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
54
Est Cost Prop Damage
0
Est Cost Emergency
15000
Est Cost Environmental
5700
Est Cost Other
0
Prpty
20754
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Preparer Name
L**** H********
Preparer Title
Dot Pipeline Safety Advisor
Preparer Email
L****************@e*********.com
Preparer Telephone
903-654-5345
Preparer Fax
903-654-5374
Prepared Date
2013-07-31 00:00:00
Authorizer Name
M*** D W******
Authorizer Telephone
713-656-0227
Authorizer Title
Manager-Safety-Health And Environmental Dept
Authorizer Email
M*************@e*********.com
Narrative
Exxonmobil personnel were on site when the incident occurred. There was a small crude stain on the soil inside the station yard. Upon excavation to check the stain, a couple of flange bolts were found loose and there was a gasket seep. The flanged bolts were torque tight, pipe section pressured up and visually inspected for any leaks. The pipeline was already down when incident occurred. Supplemental revised on 12-22-11 to correct gps coordinates in part a, removed state and county on part b, and changed g8 to g 6 equipment failure sub cause non- threaded connection failure as discussed with brian pierzina supplemental created to close the 7001 report as final. 8-22-12 7-31-13 supplemental report PHMSA requested supplemental be created to added part e 5 f data ie, ( function of pipeline system) be added to form.
| Report Received Date | 2011-04-20 00:00:00 |
|---|---|
| Iyear | 2011 |
| Report Number | 20110122 |
| Supplemental Number | 18372 |
| Report Type | Supplemental Final |
| Operator Id | 31166 PHMSA Enforcement |
| Name | Mustang Pipe Line Partners |
| Operator Street Address | 22777 Springwoods Village Parkway E2.2b-Emp |
| Operator City Name | Spring |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77389 |
| Local Datetime | 2011-03-22 09:57:00 |
| Location Latitude | 40.5161701 Google Maps OpenStreetMap |
| Location Longitude | -88.3192648 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 0.5 |
| Intentional Release Bbls | 0 |
| Recovered Bbls | 0.5 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2011-03-22 09:58:00 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | The Pipeline Was Already Down When Incident Occured And Personnel Were On Site |
| On Site Datetime | 2011-03-22 09:58:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Gibson City Pump Station, Ford County, Ill |
| Segment Name | Mustang System 18" Pipeline, Gibson City Station |
| Onshore State Abbreviation | Il |
| Onshore Postal Code | 60936 |
| Onshore City Name | Gibson City |
| Onshore County Name | Ford |
| Designated Location | Milepost/valve Station |
| Designated Name | Pump Station |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Underground |
| Pipe Facility Type | Interstate |
| Item Involved | Flange Assembly |
| Release Type | Leak |
| Leak Type | Other |
| Leak Type Other | Flange Bolt Needed Tightened. |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 54 |
| Est Cost Prop Damage | 0 |
| Est Cost Emergency | 15000 |
| Est Cost Environmental | 5700 |
| Est Cost Other | 0 |
| Prpty | 20754 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Non-Threaded Connection Failure |
| Eq Failure Type | Non-Threaded Connection Failure |
| Preparer Name | L**** H******** |
| Preparer Title | Dot Pipeline Safety Advisor |
| Preparer Email | L****************@e*********.com |
| Preparer Telephone | 903-654-5345 |
| Preparer Fax | 903-654-5374 |
| Prepared Date | 2013-07-31 00:00:00 |
| Authorizer Name | M*** D W****** |
| Authorizer Telephone | 713-656-0227 |
| Authorizer Title | Manager-Safety-Health And Environmental Dept |
| Authorizer Email | M*************@e*********.com |
| Narrative | Exxonmobil personnel were on site when the incident occurred. There was a small crude stain on the soil inside the station yard. Upon excavation to check the stain, a couple of flange bolts were found loose and there was a gasket seep. The flanged bolts were torque tight, pipe section pressured up and visually inspected for any leaks. The pipeline was already down when incident occurred. Supplemental revised on 12-22-11 to correct gps coordinates in part a, removed state and county on part b, and changed g8 to g 6 equipment failure sub cause non- threaded connection failure as discussed with brian pierzina supplemental created to close the 7001 report as final. 8-22-12 7-31-13 supplemental report PHMSA requested supplemental be created to added part e 5 f data ie, ( function of pipeline system) be added to form. |
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