HL incident on 2011-03-16 — TX

Operator
Enterprise Products Operating Llc
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2011-03-16 16:30
Report number
Location
TX
Narrative
Operator was refilling pump after draining, failed to close vent valves before product level reached vent point. Impacted soil was removed and placed in drums for proper disposal, microblaze was sprayed over the area. Reviewed filling procedure with operator and emphasized that all vent points must be checked before filling.
Detailed record list
Report Received Date
2011-03-29 00:00:00
Iyear
2011
Report Number
20110109
Supplemental Number
17609
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2011-03-16 16:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
2
Intentional Release Bbls
0
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
This Involved A Pump.
Ignite Ind
No
Explode Ind
No
Pipe Fac Name
North Port Arthur Terminal
Onshore State Abbreviation
Tx
Onshore Postal Code
77640
Onshore City Name
Port Arthur
Onshore County Name
Jefferson
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Release Type
Overfill Or Overflow
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
200
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
1000
Est Cost Other
0
Prpty
1200
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Preparer Name
J**** P* S****
Preparer Title
Pipeline Compliance Specialist
Preparer Email
J******@e****.com
Preparer Telephone
7133813614
Preparer Fax
7133816811
Prepared Date
2013-03-20 00:00:00
Authorizer Name
J**** P* S****
Authorizer Telephone
7133813614
Authorizer Title
Pipeline Compliance Specialist
Authorizer Email
J******@e****.com
Narrative
Operator was refilling pump after draining, failed to close vent valves before product level reached vent point. Impacted soil was removed and placed in drums for proper disposal, microblaze was sprayed over the area. Reviewed filling procedure with operator and emphasized that all vent points must be checked before filling.
Report Received Date 2011-03-29 00:00:00
Iyear 2011
Report Number 20110109
Supplemental Number 17609
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2011-03-16 16:30:00
Location Latitude 29.9115 Google Maps OpenStreetMap
Location Longitude -94.093194 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 2
Intentional Release Bbls 0
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain This Involved A Pump.
Ignite Ind No
Explode Ind No
Pipe Fac Name North Port Arthur Terminal
Onshore State Abbreviation Tx
Onshore Postal Code 77640
Onshore City Name Port Arthur
Onshore County Name Jefferson
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Release Type Overfill Or Overflow
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 200
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Environmental 1000
Est Cost Other 0
Prpty 1200
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Preparer Name J**** P* S****
Preparer Title Pipeline Compliance Specialist
Preparer Email J******@e****.com
Preparer Telephone 7133813614
Preparer Fax 7133816811
Prepared Date 2013-03-20 00:00:00
Authorizer Name J**** P* S****
Authorizer Telephone 7133813614
Authorizer Title Pipeline Compliance Specialist
Authorizer Email J******@e****.com
Narrative Operator was refilling pump after draining, failed to close vent valves before product level reached vent point. Impacted soil was removed and placed in drums for proper disposal, microblaze was sprayed over the area. Reviewed filling procedure with operator and emphasized that all vent points must be checked before filling.

All rights reserved. Copyright © by ClearPHMSA