Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2011-02-10 — TX
Operator
Sunoco Pipeline L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$8,370
Incident datetime
2011-02-10 08:30
Report number
Location
TX
Narrative
The spring failed on the thermal relief valve allowing the oil to overfill the sump. Re-submitted on 3/26/2013 to include part e5f per PHMSA request.
Detailed record list
Report Received Date
2011-03-10 00:00:00
Iyear
2011
Report Number
20110084
Supplemental Number
17695
Report Type
Supplemental Final
Operator Id
18718
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2011-02-10 08:30:00
Location Latitude
32.483
Location Longitude
-94.8388
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.5
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2011-02-10 08:30:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Line Segment Was Down At The Time
On Site Datetime
2011-02-10 08:30:00
Ignite Ind
No
Explode Ind
No
Pipe Fac Name
Etx 10"-Texoma Station
Segment Name
Etx 10" Meter Skid Line
Onshore State Abbreviation
Tx
Onshore Postal Code
75604
Onshore City Name
Longview
Onshore County Name
Gregg
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Relief Valve
Release Type
Overfill Or Overflow
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
42
Est Cost Prop Damage
8370
Est Cost Emergency
7973
Est Cost Environmental
2043
Est Cost Other
0
Prpty
18428
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Preparer Name
K****** D**** B***
Preparer Title
Area Dot Compliance Supervisor
Preparer Email
K*****@s**************.com
Preparer Telephone
281-637-6497
Preparer Fax
281-637-6425
Prepared Date
2013-03-26 00:00:00
Authorizer Name
K****** D**** B***
Authorizer Telephone
281-637-6497
Authorizer Title
Area Dot Compliance Supervisor
Authorizer Email
K*****@s**************.com
Narrative
The spring failed on the thermal relief valve allowing the oil to overfill the sump. Re-submitted on 3/26/2013 to include part e5f per PHMSA request.
| Report Received Date | 2011-03-10 00:00:00 |
|---|---|
| Iyear | 2011 |
| Report Number | 20110084 |
| Supplemental Number | 17695 |
| Report Type | Supplemental Final |
| Operator Id | 18718 PHMSA Enforcement |
| Name | Sunoco Pipeline L.p. |
| Operator Street Address | 1300 Main Street |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2011-02-10 08:30:00 |
| Location Latitude | 32.483 Google Maps OpenStreetMap |
| Location Longitude | -94.8388 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 0.5 |
| Intentional Release Bbls | 0 |
| Recovered Bbls | 0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2011-02-10 08:30:00 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | Line Segment Was Down At The Time |
| On Site Datetime | 2011-02-10 08:30:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Pipe Fac Name | Etx 10"-Texoma Station |
| Segment Name | Etx 10" Meter Skid Line |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 75604 |
| Onshore City Name | Longview |
| Onshore County Name | Gregg |
| Designated Location | Milepost/valve Station |
| Designated Name | 0 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Intrastate |
| Item Involved | Valve |
| Valve Type | Relief Valve |
| Release Type | Overfill Or Overflow |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 42 |
| Est Cost Prop Damage | 8370 |
| Est Cost Emergency | 7973 |
| Est Cost Environmental | 2043 |
| Est Cost Other | 0 |
| Prpty | 18428 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Malfunction Of Control/relief Equipment |
| Eq Failure Type | Malfunction Of Control/relief Equipment |
| Preparer Name | K****** D**** B*** |
| Preparer Title | Area Dot Compliance Supervisor |
| Preparer Email | K*****@s**************.com |
| Preparer Telephone | 281-637-6497 |
| Preparer Fax | 281-637-6425 |
| Prepared Date | 2013-03-26 00:00:00 |
| Authorizer Name | K****** D**** B*** |
| Authorizer Telephone | 281-637-6497 |
| Authorizer Title | Area Dot Compliance Supervisor |
| Authorizer Email | K*****@s**************.com |
| Narrative | The spring failed on the thermal relief valve allowing the oil to overfill the sump. Re-submitted on 3/26/2013 to include part e5f per PHMSA request. |
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