Incident details
Operator, cause, commodity and consequences with raw source fields.
GD incident on 2011-02-02 — SC
Operator
Fort Hill Natural Gas Auth
Cause
Excavation Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$355
Incident datetime
2011-02-02 09:16
Report number
Location
SC, OCONEE
Narrative
No narrative available.
Detailed record list
Occurred At
2011-02-02 09:16:00
Year
2011
Report Received Date
2011-03-08 00:00:00
Iyear
2011.0
Report Number
20110043.0
Supplemental Number
15211.0
Report Type
Original Final
Operator Id
5410
Name
Fort Hill Natural Gas Auth
Operator Street Address
311 S. Pendleton Street
Operator City Name
Easley
Operator State Abbreviation
SC
Operator Postal Code
29640
Local Datetime
2011-02-02 09:16:00
Location Street Address
Rochester Hwy.
Location City Name
Seneca
Location County Name
Oconee
Location State Abbreviation
SC
Location Postal Code
29678
Location Latitude
34.0
Location Longitude
-82.0
Nrc Rpt Datetime
2011-02-02 16:37:00
Nrc Rpt Num
966394
Commodity Released Type
Natural Gas
Unintentional Release
964.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
12.0
Incident Identified Datetime
2011-02-02 09:16:00
On Site Datetime
2011-02-02 09:25:00
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48.0
Crossing
No
Pipe Facility Type
Privately Owned
System Part Involved
Service
Installation Year
1952.0
Pipe Diameter
0.75
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Release Type
Other
Release Type Details
Service Tee Was Pulled Off Of Main By Excavator.
Class Location Type
Class 2 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
355.0
Est Cost Emergency
15800.0
Est Cost Other
250.0
Est Cost Other Details
Replace Service Tee And High Pressure Stand To Resident.
Est Cost Unintentional Release
8317.0
Prpty
24722.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
305.0
Accident Psig
360.0
Normal Psig
360.0
Mop Psig
400.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The pressure did not decrease in the control room and the cause was obvious.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
Notify Cga Dirt
No
Public Row Ind
Yes
Public Subtype
State Highway
Excavator Type
Contractor
Excavator Equipment
Backhoe/trackhoe
Work Performed
Sewer (Sanitary/storm)
One Call Notified Ind
Yes
One Call Ticket Num
1101310909
One Call Center Name
Sc 811
Locator Type
Contract Locator
Visible Marks
Yes
Root Cause Category
Excavation Issue
Root Cause Type
Improper Backfilling Practices
Preparer Name
L*** S******
Preparer Title
Regulatory Compliance Officer
Preparer Email
L***********@f****.com
Preparer Telephone
864 859 6375
Preparer Fax
864 850 7360
Authorizer Name
M****** L* H******
Authorizer Title
Executive V.p. And C.o.o.
Authorizer Telephone
864 859 6375
Authorizer Email
M***********@f****.com
| Occurred At | 2011-02-02 09:16:00 |
|---|---|
| Year | 2011 |
| Report Received Date | 2011-03-08 00:00:00 |
| Iyear | 2011.0 |
| Report Number | 20110043.0 |
| Supplemental Number | 15211.0 |
| Report Type | Original Final |
| Operator Id | 5410 PHMSA Enforcement |
| Name | Fort Hill Natural Gas Auth |
| Operator Street Address | 311 S. Pendleton Street |
| Operator City Name | Easley |
| Operator State Abbreviation | SC |
| Operator Postal Code | 29640 |
| Local Datetime | 2011-02-02 09:16:00 |
| Location Street Address | Rochester Hwy. |
| Location City Name | Seneca |
| Location County Name | Oconee |
| Location State Abbreviation | SC |
| Location Postal Code | 29678 |
| Location Latitude | 34.0 Google Maps OpenStreetMap |
| Location Longitude | -82.0 Google Maps OpenStreetMap |
| Nrc Rpt Datetime | 2011-02-02 16:37:00 |
| Nrc Rpt Num | 966394 NRC Report How to search |
| Commodity Released Type | Natural Gas |
| Unintentional Release | 964.0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 12.0 |
| Incident Identified Datetime | 2011-02-02 09:16:00 |
| On Site Datetime | 2011-02-02 09:25:00 |
| Federal | No |
| Location Type | Utility Right-Of-Way / Easement |
| Incident Area Type | Underground |
| Incident Area Subtype | Under Soil |
| Depth Of Cover | 48.0 |
| Crossing | No |
| Pipe Facility Type | Privately Owned |
| System Part Involved | Service |
| Installation Year | 1952.0 |
| Pipe Diameter | 0.75 |
| Pipe Specification | Unknown |
| Pipe Manufacturer | Unknown |
| Material Involved | Steel |
| Steel Seam Type | Other |
| Steel Seam Type Details | Unknown |
| Release Type | Other |
| Release Type Details | Service Tee Was Pulled Off Of Main By Excavator. |
| Class Location Type | Class 2 Location |
| Est Cost Oper Paid | 0.0 |
| Est Cost Prop Damage | 355.0 |
| Est Cost Emergency | 15800.0 |
| Est Cost Other | 250.0 |
| Est Cost Other Details | Replace Service Tee And High Pressure Stand To Resident. |
| Est Cost Unintentional Release | 8317.0 |
| Prpty | 24722.0 |
| Commercial Affected | 0.0 |
| Industrial Affected | 0.0 |
| Residences Affected | 305.0 |
| Accident Psig | 360.0 |
| Normal Psig | 360.0 |
| Mop Psig | 400.0 |
| Accident Pressure | Pressure Did Not Exceed Maop |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | No |
| Accident Identifier | Notification From Third Party That Caused The Incident |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | The pressure did not decrease in the control room and the cause was obvious. |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Excavation Damage |
| Cause Details | Excavation Damage By Third Party |
| Ex Party Type | Excavation Damage By Third Party |
| Prior Notification Ind | Yes |
| One Call System Ind | Yes |
| Notify Cga Dirt | No |
| Public Row Ind | Yes |
| Public Subtype | State Highway |
| Excavator Type | Contractor |
| Excavator Equipment | Backhoe/trackhoe |
| Work Performed | Sewer (Sanitary/storm) |
| One Call Notified Ind | Yes |
| One Call Ticket Num | 1101310909 |
| One Call Center Name | Sc 811 |
| Locator Type | Contract Locator |
| Visible Marks | Yes |
| Root Cause Category | Excavation Issue |
| Root Cause Type | Improper Backfilling Practices |
| Preparer Name | L*** S****** |
| Preparer Title | Regulatory Compliance Officer |
| Preparer Email | L***********@f****.com |
| Preparer Telephone | 864 859 6375 |
| Preparer Fax | 864 850 7360 |
| Authorizer Name | M****** L* H****** |
| Authorizer Title | Executive V.p. And C.o.o. |
| Authorizer Telephone | 864 859 6375 |
| Authorizer Email | M***********@f****.com |
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