GD incident on 2011-01-01 — AL

Operator
Alabama Gas Corporation
Cause
Pipe, Weld, Or Joint Failure
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$530
Incident datetime
2011-01-01 04:55
Report number
Location
AL, SHELBY
Narrative
A leak at the mechanical service tee resulted in the migration of natural gas into the garage area, causing an explosion. Portions of the four-unit townhome complex experienced extensive damage. The event was determined to meet the requirements of a reportable incident at approximately 9:00 a.M. In addition to the figures provided in part d of this report, the incident has forced alabama gas to undergo inspection and remediation efforts for similarly defective and mis-installed tapping tees throughout the narrows and other subdivisions. These efforts are currently underway, and they are expected to take another 8 years to complete. Alabama gas spent approximately $854,669.00 as part of its inspection and remediation efforts at the narrows, and costs associated with the entire inspection and remediation project are estimated to be approximately $20 million.
Detailed record list
Occurred At
2011-01-01 04:55:00
Year
2011
Report Received Date
2011-01-28 00:00:00
Iyear
2011.0
Report Number
20110016.0
Supplemental Number
16174.0
Report Type
Supplemental Final
Operator Id
Name
Alabama Gas Corporation
Operator Street Address
605 Richard Arrington Jr Blvd N
Operator City Name
Birmingham
Operator State Abbreviation
AL
Operator Postal Code
35203
Local Datetime
2011-01-01 04:42:00
Location Street Address
301 Reach Court
Location City Name
Birmingham
Location County Name
Shelby
Location State Abbreviation
AL
Location Postal Code
35242
Location Latitude
Location Longitude
Nrc Rpt Datetime
2011-01-01 09:25:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
6.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
Yes
Explode Ind
Yes
Num Pub Evacuated
5.0
Incident Identified Datetime
2011-01-01 04:55:00
On Site Datetime
2011-01-01 05:27:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
36.0
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Other
System Part Details
Service Tap
Installation Year
2002.0
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Wt Plastic Unknown Ind
Unknown
Material Pe Pipe Code
2406
Release Type
Leak
Leak Type
Connection Failure
Class Location Type
Class 3 Location
Est Cost Oper Paid
731160.0
Est Cost Prop Damage
530.0
Est Cost Emergency
1500.0
Est Cost Other
15617.0
Est Cost Other Details
Investigative Costs
Est Cost Unintentional Release
80.0
Prpty
748887.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
10.0
Accident Psig
40.0
Normal Psig
40.0
Mop Psig
60.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Volume of lost gas was not enough to distinguish a problem.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Pipe, Weld, Or Joint Failure
Cause Details
Mechanical Joint Failure
Pwjf Failure Type
Mechanical Joint Failure
Mec Fitting Involved
Bolted
Mec Fitting Type
Service Or Main Tee
Mec Manufacturer
Perfection
Mec Fitting Material
Other
Mec Fitting Material Detail
Materials Joined: 1st Plastic, 2nd Plastic
Additional Other Ind
Yes
Additional Factor Details
The Operator's Ongoing Analysis Concludes That The Manufacturer's Design Contributed To This Incident.
Result Construction Ind
Yes
Result Construction Subtype
Procedure Not Followed
Hydrotest Conducted Ind
No
Preparer Name
R**** A* W*****
Preparer Title
Manager-Regulatory Compliance
Preparer Email
R***********@a*******.com
Preparer Telephone
205-326-2987
Preparer Fax
205-326-8483
Authorizer Name
R***** N* G******
Authorizer Title
Director-Quality Assurance And Compliance
Authorizer Telephone
205-326-2584
Authorizer Email
B**********@a*******.com
Narrative
A leak at the mechanical service tee resulted in the migration of natural gas into the garage area, causing an explosion. Portions of the four-unit townhome complex experienced extensive damage. The event was determined to meet the requirements of a reportable incident at approximately 9:00 a.M. In addition to the figures provided in part d of this report, the incident has forced alabama gas to undergo inspection and remediation efforts for similarly defective and mis-installed tapping tees throughout the narrows and other subdivisions. These efforts are currently underway, and they are expected to take another 8 years to complete. Alabama gas spent approximately $854,669.00 as part of its inspection and remediation efforts at the narrows, and costs associated with the entire inspection and remediation project are estimated to be approximately $20 million.
Occurred At 2011-01-01 04:55:00
Year 2011
Report Received Date 2011-01-28 00:00:00
Iyear 2011.0
Report Number 20110016.0
Supplemental Number 16174.0
Report Type Supplemental Final
Operator Id 180 PHMSA Enforcement
Name Alabama Gas Corporation
Operator Street Address 605 Richard Arrington Jr Blvd N
Operator City Name Birmingham
Operator State Abbreviation AL
Operator Postal Code 35203
Local Datetime 2011-01-01 04:42:00
Location Street Address 301 Reach Court
Location City Name Birmingham
Location County Name Shelby
Location State Abbreviation AL
Location Postal Code 35242
Location Latitude 33.37117 Google Maps OpenStreetMap
Location Longitude -86.66799 Google Maps OpenStreetMap
Nrc Rpt Datetime 2011-01-01 09:25:00
Nrc Rpt Num 963465 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 6.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind Yes
Explode Ind Yes
Num Pub Evacuated 5.0
Incident Identified Datetime 2011-01-01 04:55:00
On Site Datetime 2011-01-01 05:27:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Under Pavement
Depth Of Cover 36.0
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Other
System Part Details Service Tap
Installation Year 2002.0
Material Involved Plastic
Plastic Type Polyethylene (Pe)
Wt Plastic Unknown Ind Unknown
Material Pe Pipe Code 2406
Release Type Leak
Leak Type Connection Failure
Class Location Type Class 3 Location
Est Cost Oper Paid 731160.0
Est Cost Prop Damage 530.0
Est Cost Emergency 1500.0
Est Cost Other 15617.0
Est Cost Other Details Investigative Costs
Est Cost Unintentional Release 80.0
Prpty 748887.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 10.0
Accident Psig 40.0
Normal Psig 40.0
Mop Psig 60.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Volume of lost gas was not enough to distinguish a problem.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Pipe, Weld, Or Joint Failure
Cause Details Mechanical Joint Failure
Pwjf Failure Type Mechanical Joint Failure
Mec Fitting Involved Bolted
Mec Fitting Type Service Or Main Tee
Mec Manufacturer Perfection
Mec Fitting Material Other
Mec Fitting Material Detail Materials Joined: 1st Plastic, 2nd Plastic
Additional Other Ind Yes
Additional Factor Details The Operator's Ongoing Analysis Concludes That The Manufacturer's Design Contributed To This Incident.
Result Construction Ind Yes
Result Construction Subtype Procedure Not Followed
Hydrotest Conducted Ind No
Preparer Name R**** A* W*****
Preparer Title Manager-Regulatory Compliance
Preparer Email R***********@a*******.com
Preparer Telephone 205-326-2987
Preparer Fax 205-326-8483
Authorizer Name R***** N* G******
Authorizer Title Director-Quality Assurance And Compliance
Authorizer Telephone 205-326-2584
Authorizer Email B**********@a*******.com
Narrative A leak at the mechanical service tee resulted in the migration of natural gas into the garage area, causing an explosion. Portions of the four-unit townhome complex experienced extensive damage. The event was determined to meet the requirements of a reportable incident at approximately 9:00 a.M. In addition to the figures provided in part d of this report, the incident has forced alabama gas to undergo inspection and remediation efforts for similarly defective and mis-installed tapping tees throughout the narrows and other subdivisions. These efforts are currently underway, and they are expected to take another 8 years to complete. Alabama gas spent approximately $854,669.00 as part of its inspection and remediation efforts at the narrows, and costs associated with the entire inspection and remediation project are estimated to be approximately $20 million.

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