Incident details
Operator, cause, commodity and consequences with raw source fields.
GD incident on 2010-12-23 — LA
Operator
Grand Isle, Town Of
Cause
Incorrect Operation
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities
2 injuries
Property damage (nominal)
$0
Incident datetime
2010-12-23 09:18
Report number
Location
LA, JEFFERSON PARISH
Narrative
While installing a poly valve assenbly on a 2" flanged steel pipe static electricity ignited the escaping gas.
Detailed record list
Occurred At
2010-12-23 09:18:00
Year
2010
Report Received Date
2011-01-24 00:00:00
Iyear
2010.0
Report Number
20110012.0
Supplemental Number
15249.0
Report Type
Supplemental Final
Operator Id
6510
Name
Grand Isle, Town Of
Operator Street Address
Po Box 200
Operator City Name
Grand Isle
Operator State Abbreviation
LA
Operator Postal Code
70358
Local Datetime
2010-12-23 09:18:00
Location Street Address
La 1 & Central
Location City Name
Grand Isle
Location County Name
Jefferson Parish
Location State Abbreviation
LA
Location Postal Code
70356
Location Latitude
29.210117
Location Longitude
-90.050133
Nrc Rpt Datetime
2010-12-28 13:00:00
Commodity Released Type
Natural Gas
Unintentional Release
139.0
Fatality Ind
No
Fatal
0
Injury Ind
Yes
Num Emp Injuries
0
Num Contr Injuries
2
Num Er Injuries
0
Num Worker Injuries
0
Num Gp Injuries
0
Injure
2
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2010-12-23 09:18:00
On Site Datetime
2010-12-23 09:18:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Crossing
No
Pipe Facility Type
Municipally Owned
System Part Involved
Main
Installation Year
1974.0
Pipe Diameter
2.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Release Type
Other
Release Type Details
2" Pipe Cut To Install Valve
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
0.0
Est Cost Emergency
1000.0
Est Cost Other
0.0
Est Cost Unintentional Release
695.0
Prpty
1695.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
100.0
Accident Psig
45.0
Normal Psig
45.0
Mop Psig
60.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
Prevention Of Accidential Ignition
Related Other Ind
Yes
Operation Related Details
Failure To Secure Wet Rag To Pe Pipe
Category Type
Construction
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
G***** M******** J*
Authorizer Name
G***** M******** J*
Authorizer Telephone
504-891-4711
Narrative
While installing a poly valve assenbly on a 2" flanged steel pipe static electricity ignited the escaping gas.
| Occurred At | 2010-12-23 09:18:00 |
|---|---|
| Year | 2010 |
| Report Received Date | 2011-01-24 00:00:00 |
| Iyear | 2010.0 |
| Report Number | 20110012.0 |
| Supplemental Number | 15249.0 |
| Report Type | Supplemental Final |
| Operator Id | 6510 PHMSA Enforcement |
| Name | Grand Isle, Town Of |
| Operator Street Address | Po Box 200 |
| Operator City Name | Grand Isle |
| Operator State Abbreviation | LA |
| Operator Postal Code | 70358 |
| Local Datetime | 2010-12-23 09:18:00 |
| Location Street Address | La 1 & Central |
| Location City Name | Grand Isle |
| Location County Name | Jefferson Parish |
| Location State Abbreviation | LA |
| Location Postal Code | 70356 |
| Location Latitude | 29.210117 Google Maps OpenStreetMap |
| Location Longitude | -90.050133 Google Maps OpenStreetMap |
| Nrc Rpt Datetime | 2010-12-28 13:00:00 |
| Commodity Released Type | Natural Gas |
| Unintentional Release | 139.0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | Yes |
| Num Emp Injuries | 0 |
| Num Contr Injuries | 2 |
| Num Er Injuries | 0 |
| Num Worker Injuries | 0 |
| Num Gp Injuries | 0 |
| Injure | 2 |
| Ignite Ind | Yes |
| Explode Ind | No |
| Num Pub Evacuated | 0.0 |
| Incident Identified Datetime | 2010-12-23 09:18:00 |
| On Site Datetime | 2010-12-23 09:18:00 |
| Federal | No |
| Location Type | Public Property |
| Incident Area Type | Underground |
| Incident Area Subtype | Exposed Due To Excavation |
| Crossing | No |
| Pipe Facility Type | Municipally Owned |
| System Part Involved | Main |
| Installation Year | 1974.0 |
| Pipe Diameter | 2.0 |
| Pipe Specification | Unknown |
| Pipe Manufacturer | Unknown |
| Material Involved | Steel |
| Steel Seam Type | Other |
| Steel Seam Type Details | Unknown |
| Release Type | Other |
| Release Type Details | 2" Pipe Cut To Install Valve |
| Class Location Type | Class 3 Location |
| Est Cost Oper Paid | 0.0 |
| Est Cost Prop Damage | 0.0 |
| Est Cost Emergency | 1000.0 |
| Est Cost Other | 0.0 |
| Est Cost Unintentional Release | 695.0 |
| Prpty | 1695.0 |
| Commercial Affected | 0.0 |
| Industrial Affected | 0.0 |
| Residences Affected | 100.0 |
| Accident Psig | 45.0 |
| Normal Psig | 45.0 |
| Mop Psig | 60.0 |
| Accident Pressure | Pressure Did Not Exceed Maop |
| Scada In Place Ind | No |
| Accident Identifier | Notification From Third Party That Caused The Incident |
| Investigation Status | No, the facility was not monitored by a controller(s) at the time of the incident |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Incorrect Operation |
| Cause Details | Other Incorrect Operation |
| Operation Type | Other Incorrect Operation |
| Operation Details | Prevention Of Accidential Ignition |
| Related Other Ind | Yes |
| Operation Related Details | Failure To Secure Wet Rag To Pe Pipe |
| Category Type | Construction |
| Operator Qualification Ind | Yes |
| Qualified Individuals | Yes, They Were Qualified For The Task(S) |
| Preparer Name | G***** M******** J* |
| Authorizer Name | G***** M******** J* |
| Authorizer Telephone | 504-891-4711 |
| Narrative | While installing a poly valve assenbly on a 2" flanged steel pipe static electricity ignited the escaping gas. |
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