HL incident on 2010-12-02 — PA

Operator
Buckeye Partners, Lp
Cause
Other Outside Force Damage
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$188,580
Incident datetime
2010-12-02 19:50
Report number
Location
PA
Narrative
At approximately 7:15 pm on december 2, 2010, buckeye's control center received a call from the local fire department in madison co., il reporting a petroleum odor in the area of one of buckeye's pipelines. The control center had no alarms on the leakwarn system and dispatched local personnel to check the area. Local buckeye personnel arrived in the area at approximately 7:50 pm, confirmed the release, and shut down the pipeline. Buckeye immediately initiated emergency response procedures to contain the release & minimize environmental impact. Buckeye excavated the affected area and found mechanical damage to the pipe, possibly from a farm plow. During the excavation work, several more instances of mechanical damage were found. As a result of the damage, approximately 266' of pipe was cut out and replaced with certified pipe. The pipeline repairs have been completed and the line was restarted on december 9, 2010. The section of pipe where the release occurred has been sent to a laboratory for metallurgical analysis to determine the cause. Environmental remediation is ongoing. Metallurgical analysis has determined the cause of the release to be failure due to ductile overload stemming from external mechanical damage. Remediation is still ongoing. 12/16/2013: remediation charges updated. Volumes unchanged at this time 07/21/2015: remediation charges updated. Volumes unchanged at this time 08/02/2016: updated nrc call time to 20:39. Updated nominal size to 8" instead of 8.625 08/08/16: updated a4 to 19:15. Buckeye received an odor complaint call at 19:15 (ct). The complaint was immediately investigated and a buckeye employee had confirmed discovery at 19:50 (ct).
Detailed record list
Report Received Date
2010-12-29 00:00:00
Iyear
2010
Report Number
20100315
Supplemental Number
22011
Report Type
Supplemental Final
Operator Id
Name
Buckeye Partners, Lp
Operator Street Address
The Buckeye Building 6161 Hamilton Boulevar
Operator City Name
Allentown
Operator State Abbreviation
PA
Operator Postal Code
18106
Local Datetime
2010-12-02 19:15:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
500
Intentional Release Bbls
0
Recovered Bbls
10.3
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Emergency Responder
Incident Identified Datetime
2010-12-02 19:50:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2010-12-02 19:50:00
Restart Datetime
2010-12-09 22:10:00
On Site Datetime
2010-12-02 19:50:00
Nrc Rpt Datetime
2010-12-02 20:59:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Sauget To Dupo 162 Line
Segment Name
Sg162du
Onshore State Abbreviation
Il
Onshore Postal Code
62097
Onshore City Name
New Douglas
Onshore County Name
Madison
Designated Location
Milepost/valve Station
Designated Name
3839912
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
Unknown
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8
Pipe Wall Thickness
0.188
Pipe Smys
42000
Pipe Specification
Api 5l X-42
Pipe Seam Type
Erw � Unknown Frequency
Pipe Manufacturer
Republic
Pipe Coating Type
Coal Tar
Installation Year
1951
Manufactured Year
1951
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Surface Water Remed Ind
Yes
Groundwater Remed Ind
Yes
Soil Remed Ind
Yes
Vegetation Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Groundwater Contam Ind
Yes
Amount Released
5
Rel Water Name
Private Farm Pond Which Flows Into An Unnamed Tributary Of Silver Creek
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
50000
Est Cost Prop Damage
188580
Est Cost Emergency
666080
Est Cost Environmental
3804906
Est Cost Other
0
Prpty
4709566
Accident Psig
456
Mop Psig
960
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
170259
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
This was a small release over an extended period, so the controllers and leakwarn system couldn't detect it
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Outside Force Damage
Cause Details
Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Outside Force Type
Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Vehicle Subtype
Third Party
Preparer Name
C****** P********
Preparer Title
Director Regulatory Compliance
Preparer Email
C*********@b******.com
Preparer Telephone
610-904-4113
Prepared Date
2017-01-10 00:00:00
Authorizer Name
C****** P********
Authorizer Telephone
610-904-4113
Authorizer Title
Director Regulatory Compliance
Authorizer Email
C*********@b******.com
Narrative
At approximately 7:15 pm on december 2, 2010, buckeye's control center received a call from the local fire department in madison co., il reporting a petroleum odor in the area of one of buckeye's pipelines. The control center had no alarms on the leakwarn system and dispatched local personnel to check the area. Local buckeye personnel arrived in the area at approximately 7:50 pm, confirmed the release, and shut down the pipeline. Buckeye immediately initiated emergency response procedures to contain the release & minimize environmental impact. Buckeye excavated the affected area and found mechanical damage to the pipe, possibly from a farm plow. During the excavation work, several more instances of mechanical damage were found. As a result of the damage, approximately 266' of pipe was cut out and replaced with certified pipe. The pipeline repairs have been completed and the line was restarted on december 9, 2010. The section of pipe where the release occurred has been sent to a laboratory for metallurgical analysis to determine the cause. Environmental remediation is ongoing. Metallurgical analysis has determined the cause of the release to be failure due to ductile overload stemming from external mechanical damage. Remediation is still ongoing. 12/16/2013: remediation charges updated. Volumes unchanged at this time 07/21/2015: remediation charges updated. Volumes unchanged at this time 08/02/2016: updated nrc call time to 20:39. Updated nominal size to 8" instead of 8.625 08/08/16: updated a4 to 19:15. Buckeye received an odor complaint call at 19:15 (ct). The complaint was immediately investigated and a buckeye employee had confirmed discovery at 19:50 (ct).
Report Received Date 2010-12-29 00:00:00
Iyear 2010
Report Number 20100315
Supplemental Number 22011
Report Type Supplemental Final
Operator Id 1845 PHMSA Enforcement
Name Buckeye Partners, Lp
Operator Street Address The Buckeye Building 6161 Hamilton Boulevar
Operator City Name Allentown
Operator State Abbreviation PA
Operator Postal Code 18106
Local Datetime 2010-12-02 19:15:00
Location Latitude 38.94905 Google Maps OpenStreetMap
Location Longitude -89.75185 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 500
Intentional Release Bbls 0
Recovered Bbls 10.3
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Emergency Responder
Incident Identified Datetime 2010-12-02 19:50:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2010-12-02 19:50:00
Restart Datetime 2010-12-09 22:10:00
On Site Datetime 2010-12-02 19:50:00
Nrc Rpt Datetime 2010-12-02 20:59:00
Nrc Rpt Num 961279 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Sauget To Dupo 162 Line
Segment Name Sg162du
Onshore State Abbreviation Il
Onshore Postal Code 62097
Onshore City Name New Douglas
Onshore County Name Madison
Designated Location Milepost/valve Station
Designated Name 3839912
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover Unknown
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 8
Pipe Wall Thickness 0.188
Pipe Smys 42000
Pipe Specification Api 5l X-42
Pipe Seam Type Erw � Unknown Frequency
Pipe Manufacturer Republic
Pipe Coating Type Coal Tar
Installation Year 1951
Manufactured Year 1951
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Surface Water Remed Ind Yes
Groundwater Remed Ind Yes
Soil Remed Ind Yes
Vegetation Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Groundwater Contam Ind Yes
Amount Released 5
Rel Water Name Private Farm Pond Which Flows Into An Unnamed Tributary Of Silver Creek
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 50000
Est Cost Prop Damage 188580
Est Cost Emergency 666080
Est Cost Environmental 3804906
Est Cost Other 0
Prpty 4709566
Accident Psig 456
Mop Psig 960
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 170259
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details This was a small release over an extended period, so the controllers and leakwarn system couldn't detect it
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Outside Force Damage
Cause Details Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Outside Force Type Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Vehicle Subtype Third Party
Preparer Name C****** P********
Preparer Title Director Regulatory Compliance
Preparer Email C*********@b******.com
Preparer Telephone 610-904-4113
Prepared Date 2017-01-10 00:00:00
Authorizer Name C****** P********
Authorizer Telephone 610-904-4113
Authorizer Title Director Regulatory Compliance
Authorizer Email C*********@b******.com
Narrative At approximately 7:15 pm on december 2, 2010, buckeye's control center received a call from the local fire department in madison co., il reporting a petroleum odor in the area of one of buckeye's pipelines. The control center had no alarms on the leakwarn system and dispatched local personnel to check the area. Local buckeye personnel arrived in the area at approximately 7:50 pm, confirmed the release, and shut down the pipeline. Buckeye immediately initiated emergency response procedures to contain the release & minimize environmental impact. Buckeye excavated the affected area and found mechanical damage to the pipe, possibly from a farm plow. During the excavation work, several more instances of mechanical damage were found. As a result of the damage, approximately 266' of pipe was cut out and replaced with certified pipe. The pipeline repairs have been completed and the line was restarted on december 9, 2010. The section of pipe where the release occurred has been sent to a laboratory for metallurgical analysis to determine the cause. Environmental remediation is ongoing. Metallurgical analysis has determined the cause of the release to be failure due to ductile overload stemming from external mechanical damage. Remediation is still ongoing. 12/16/2013: remediation charges updated. Volumes unchanged at this time 07/21/2015: remediation charges updated. Volumes unchanged at this time 08/02/2016: updated nrc call time to 20:39. Updated nominal size to 8" instead of 8.625 08/08/16: updated a4 to 19:15. Buckeye received an odor complaint call at 19:15 (ct). The complaint was immediately investigated and a buckeye employee had confirmed discovery at 19:50 (ct).

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