Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2010-11-15 — KS
Operator
Jayhawk Pipeline Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$0
Incident datetime
2010-11-15 08:35
Report number
Location
KS
Narrative
Supplemental was filed to provide narration and clear up why there were no costs associated with regards to remediation. As to this matter I did not show any remediation costs because while there was no standing water the ground was extremely saturated from recent and heavy rains. The ground was so wet that when vacuum truck arrived they picked up all oil either from concrete pump base or off the top of the ground. As to narration of incident. A third party truck driver unloading crude at the site saw small area of oil around pump coming from the packing area, he notified company personnel and they inturn called vacuum truck. Upon arrival at site company personnel found packing had began to fail and ran over the small "sump" connected to the packing/seal cavity and spilled onto concrete base and wet ground. Mechanic was called, oil was picked up immediately and when pump was repacked pump was restarted.
Detailed record list
Report Received Date
2010-12-16 00:00:00
Iyear
2010
Report Number
20100304
Supplemental Number
18139
Report Type
Supplemental Final
Operator Id
9175
Name
Jayhawk Pipeline Llc
Operator Street Address
2000 South Main
Operator City Name
Mcpherson
Operator State Abbreviation
KS
Operator Postal Code
67460
Local Datetime
2010-11-15 08:35:00
Location Latitude
37.414383
Location Longitude
-99.320819
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Intentional Release Bbls
0
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2010-11-15 08:36:00
Restart Datetime
2010-11-15 12:45:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Coldwater Station
Segment Name
Harper Ranch To Haviland
Onshore State Abbreviation
Ks
Onshore Postal Code
67209
Onshore City Name
Coldwater
Onshore County Name
Kiowa
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Pump
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
0
Est Cost Emergency
300
Est Cost Environmental
0
Est Cost Other
0
Prpty
300
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Preparer Name
D**** C***
Preparer Title
Operations Manager
Preparer Email
D****@j********.com
Preparer Telephone
620-241-9260
Preparer Fax
620-241-9215
Prepared Date
2013-05-29 00:00:00
Authorizer Name
D**** C***
Authorizer Telephone
620-241-9260
Authorizer Title
Operatiions Manager
Authorizer Email
D****@j********.com
Narrative
Supplemental was filed to provide narration and clear up why there were no costs associated with regards to remediation. As to this matter I did not show any remediation costs because while there was no standing water the ground was extremely saturated from recent and heavy rains. The ground was so wet that when vacuum truck arrived they picked up all oil either from concrete pump base or off the top of the ground. As to narration of incident. A third party truck driver unloading crude at the site saw small area of oil around pump coming from the packing area, he notified company personnel and they inturn called vacuum truck. Upon arrival at site company personnel found packing had began to fail and ran over the small "sump" connected to the packing/seal cavity and spilled onto concrete base and wet ground. Mechanic was called, oil was picked up immediately and when pump was repacked pump was restarted.
| Report Received Date | 2010-12-16 00:00:00 |
|---|---|
| Iyear | 2010 |
| Report Number | 20100304 |
| Supplemental Number | 18139 |
| Report Type | Supplemental Final |
| Operator Id | 9175 PHMSA Enforcement |
| Name | Jayhawk Pipeline Llc |
| Operator Street Address | 2000 South Main |
| Operator City Name | Mcpherson |
| Operator State Abbreviation | KS |
| Operator Postal Code | 67460 |
| Local Datetime | 2010-11-15 08:35:00 |
| Location Latitude | 37.414383 Google Maps OpenStreetMap |
| Location Longitude | -99.320819 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 2 |
| Intentional Release Bbls | 0 |
| Recovered Bbls | 2 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2010-11-15 08:36:00 |
| Restart Datetime | 2010-11-15 12:45:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Coldwater Station |
| Segment Name | Harper Ranch To Haviland |
| Onshore State Abbreviation | Ks |
| Onshore Postal Code | 67209 |
| Onshore City Name | Coldwater |
| Onshore County Name | Kiowa |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Interstate |
| Item Involved | Pump |
| Release Type | Leak |
| Leak Type | Seal Or Packing |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 0 |
| Est Cost Prop Damage | 0 |
| Est Cost Emergency | 300 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 300 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Pump Or Pump-Related Equipment |
| Eq Failure Type | Pump Or Pump-Related Equipment |
| Preparer Name | D**** C*** |
| Preparer Title | Operations Manager |
| Preparer Email | D****@j********.com |
| Preparer Telephone | 620-241-9260 |
| Preparer Fax | 620-241-9215 |
| Prepared Date | 2013-05-29 00:00:00 |
| Authorizer Name | D**** C*** |
| Authorizer Telephone | 620-241-9260 |
| Authorizer Title | Operatiions Manager |
| Authorizer Email | D****@j********.com |
| Narrative | Supplemental was filed to provide narration and clear up why there were no costs associated with regards to remediation. As to this matter I did not show any remediation costs because while there was no standing water the ground was extremely saturated from recent and heavy rains. The ground was so wet that when vacuum truck arrived they picked up all oil either from concrete pump base or off the top of the ground. As to narration of incident. A third party truck driver unloading crude at the site saw small area of oil around pump coming from the packing area, he notified company personnel and they inturn called vacuum truck. Upon arrival at site company personnel found packing had began to fail and ran over the small "sump" connected to the packing/seal cavity and spilled onto concrete base and wet ground. Mechanic was called, oil was picked up immediately and when pump was repacked pump was restarted. |
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