HL incident on 2010-11-20 — TX

Operator
Kinder Morgan Liquid Terminals, Llc
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2010-11-20 08:55
Report number
Location
TX
Narrative
Operator opened small sample line valve to sample inbound receipt. There was no flow due to the line being temporarily shut down. The operator left area to perform other duties but neglected to close the sample line valve. The inbound receipt started up while the operator was away and product flowed out of the sample line into a collection tube and then the collection tub overflowed prior to another employee discovering the problem who then closed the valve and alerted the control room.
Detailed record list
Report Received Date
2010-12-14 00:00:00
Iyear
2010
Report Number
20100301
Supplemental Number
18056
Report Type
Supplemental Final
Operator Id
Name
Kinder Morgan Liquid Terminals, Llc
Operator Street Address
1001 Louisiana St, Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2010-11-20 08:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
4
Intentional Release Bbls
0
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2010-11-20 08:55:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2010-11-20 08:55:00
Restart Datetime
2010-11-20 11:30:00
On Site Datetime
2010-11-20 09:30:00
Ignite Ind
No
Explode Ind
No
Pipe Fac Name
Carteret Terminal In Plant Colonial Connection
Segment Name
Colonial Km1 Connection
Onshore State Abbreviation
Nj
Onshore Postal Code
07008
Onshore City Name
Carteret
Onshore County Name
Middlesex
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Intrastate
Item Involved
Auxiliary Piping (E.g. Drain Lines)
Release Type
Leak
Leak Type
Other
Leak Type Other
Operational Error
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
200
Est Cost Prop Damage
0
Est Cost Emergency
5500
Est Cost Environmental
6000
Est Cost Other
0
Prpty
11700
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Preparer Name
J**** H*****
Preparer Title
Pipeline Integrity Manager
Preparer Email
J***********@k***********.com
Preparer Telephone
732-969-5735
Prepared Date
2013-05-15 00:00:00
Authorizer Name
J**** H*****
Authorizer Telephone
732-969-5735
Authorizer Title
Pipeline Integrity Manager
Authorizer Email
J***********@k***********.com
Narrative
Operator opened small sample line valve to sample inbound receipt. There was no flow due to the line being temporarily shut down. The operator left area to perform other duties but neglected to close the sample line valve. The inbound receipt started up while the operator was away and product flowed out of the sample line into a collection tube and then the collection tub overflowed prior to another employee discovering the problem who then closed the valve and alerted the control room.
Report Received Date 2010-12-14 00:00:00
Iyear 2010
Report Number 20100301
Supplemental Number 18056
Report Type Supplemental Final
Operator Id 26041 PHMSA Enforcement
Name Kinder Morgan Liquid Terminals, Llc
Operator Street Address 1001 Louisiana St, Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2010-11-20 08:30:00
Location Latitude 40.58925 Google Maps OpenStreetMap
Location Longitude -74.21709 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 4
Intentional Release Bbls 0
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2010-11-20 08:55:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2010-11-20 08:55:00
Restart Datetime 2010-11-20 11:30:00
On Site Datetime 2010-11-20 09:30:00
Ignite Ind No
Explode Ind No
Pipe Fac Name Carteret Terminal In Plant Colonial Connection
Segment Name Colonial Km1 Connection
Onshore State Abbreviation Nj
Onshore Postal Code 07008
Onshore City Name Carteret
Onshore County Name Middlesex
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Pipe Facility Type Intrastate
Item Involved Auxiliary Piping (E.g. Drain Lines)
Release Type Leak
Leak Type Other
Leak Type Other Operational Error
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 200
Est Cost Prop Damage 0
Est Cost Emergency 5500
Est Cost Environmental 6000
Est Cost Other 0
Prpty 11700
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Preparer Name J**** H*****
Preparer Title Pipeline Integrity Manager
Preparer Email J***********@k***********.com
Preparer Telephone 732-969-5735
Prepared Date 2013-05-15 00:00:00
Authorizer Name J**** H*****
Authorizer Telephone 732-969-5735
Authorizer Title Pipeline Integrity Manager
Authorizer Email J***********@k***********.com
Narrative Operator opened small sample line valve to sample inbound receipt. There was no flow due to the line being temporarily shut down. The operator left area to perform other duties but neglected to close the sample line valve. The inbound receipt started up while the operator was away and product flowed out of the sample line into a collection tube and then the collection tub overflowed prior to another employee discovering the problem who then closed the valve and alerted the control room.

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