HL incident on 2010-12-09 — IL

Operator
Amoco Oil Co
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$250
Incident datetime
2010-12-09 11:50
Report number
Location
IL
Narrative
On dec 9, 2010, upon return to wood river pipeline station, the technician noticed stained gravel around the booster pump. The seal on the booster pump had failed. The technician isolated the pump to stop the flow of product from the pump. The station was down at the time the leak was discovered. The technician notified his team leader and began making arrangements to have the impacted area cleaned up. The estimated volume release was .23 barrels.
Detailed record list
Report Received Date
2010-12-13 00:00:00
Iyear
2010
Report Number
20100298
Supplemental Number
17548
Report Type
Supplemental Final
Operator Id
Name
Amoco Oil Co
Operator Street Address
150 Warrenville Road
Operator City Name
Naperville
Operator State Abbreviation
IL
Operator Postal Code
60563
Local Datetime
2010-12-09 11:50:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
0.23
Intentional Release Bbls
0
Recovered Bbls
0.23
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2010-12-09 11:50:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Line Was Already Down
On Site Datetime
2010-12-09 11:50:00
Nrc Rpt Datetime
2010-12-09 14:34:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Wood River Pump Station
Segment Name
Wood River To Milan Segment
Onshore State Abbreviation
Il
Onshore Postal Code
62095
Onshore City Name
Wood River
Onshore County Name
Madison
Designated Location
Milepost/valve Station
Designated Name
Mp163.97
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Pump
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
50
Est Cost Prop Damage
250
Est Cost Emergency
150
Est Cost Environmental
3000
Est Cost Other
0
Prpty
3450
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Preparer Name
S**** F*********
Preparer Title
Dot Compliance Advisor
Preparer Email
F*****@b*.com
Preparer Telephone
281-217-3703
Preparer Fax
281-366-3398
Prepared Date
2013-03-15 00:00:00
Authorizer Name
R** K*******
Authorizer Telephone
630-536-2549
Authorizer Title
Dot Compliance Team Leader
Authorizer Email
K*******@b*.com
Narrative
On dec 9, 2010, upon return to wood river pipeline station, the technician noticed stained gravel around the booster pump. The seal on the booster pump had failed. The technician isolated the pump to stop the flow of product from the pump. The station was down at the time the leak was discovered. The technician notified his team leader and began making arrangements to have the impacted area cleaned up. The estimated volume release was .23 barrels.
Report Received Date 2010-12-13 00:00:00
Iyear 2010
Report Number 20100298
Supplemental Number 17548
Report Type Supplemental Final
Operator Id 395 PHMSA Enforcement
Name Amoco Oil Co
Operator Street Address 150 Warrenville Road
Operator City Name Naperville
Operator State Abbreviation IL
Operator Postal Code 60563
Local Datetime 2010-12-09 11:50:00
Location Latitude 38.848525 Google Maps OpenStreetMap
Location Longitude -90.084617 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 0.23
Intentional Release Bbls 0
Recovered Bbls 0.23
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2010-12-09 11:50:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Line Was Already Down
On Site Datetime 2010-12-09 11:50:00
Nrc Rpt Datetime 2010-12-09 14:34:00
Nrc Rpt Num 961818 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Wood River Pump Station
Segment Name Wood River To Milan Segment
Onshore State Abbreviation Il
Onshore Postal Code 62095
Onshore City Name Wood River
Onshore County Name Madison
Designated Location Milepost/valve Station
Designated Name Mp163.97
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Pipe Facility Type Interstate
Item Involved Pump
Release Type Leak
Leak Type Seal Or Packing
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 50
Est Cost Prop Damage 250
Est Cost Emergency 150
Est Cost Environmental 3000
Est Cost Other 0
Prpty 3450
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Preparer Name S**** F*********
Preparer Title Dot Compliance Advisor
Preparer Email F*****@b*.com
Preparer Telephone 281-217-3703
Preparer Fax 281-366-3398
Prepared Date 2013-03-15 00:00:00
Authorizer Name R** K*******
Authorizer Telephone 630-536-2549
Authorizer Title Dot Compliance Team Leader
Authorizer Email K*******@b*.com
Narrative On dec 9, 2010, upon return to wood river pipeline station, the technician noticed stained gravel around the booster pump. The seal on the booster pump had failed. The technician isolated the pump to stop the flow of product from the pump. The station was down at the time the leak was discovered. The technician notified his team leader and began making arrangements to have the impacted area cleaned up. The estimated volume release was .23 barrels.

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