HL incident on 2010-11-12 — OK

Operator
Magellan Pipeline Company, Lp
Cause
Material Failure Of Pipe Or Weld
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$33,000
Incident datetime
2010-11-12 09:48
Report number
Location
OK
Narrative
Magellan's northern district office was notified of a reported sheen on water in a drainage ditch by the minnesota pollution control agency. The northern district office informed magellan's operations control center whereupon the line was immediately shut down. Up-and-down stream valves were closed and a ground search was conducted which included excavating the line in the vicinity of the reported sighting. A large rock was discovered immediately under the pipeline. When the rock was removed a leak was discovered on the bottom of the pipe which had been resting on the rock. Metallurgical analysis determined the cause of the release as a through the wall crack in a bottom side deformation anomaly that grew from mechanical damage on the inside surface of the pipe.
Detailed record list
Report Received Date
2010-12-10 00:00:00
Iyear
2010
Report Number
20100290
Supplemental Number
15722
Report Type
Supplemental Final
Operator Id
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2010-11-12 09:48:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
48
Intentional Release Bbls
0
Recovered Bbls
48
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Minnesota Pollution Control Agency
Incident Identified Datetime
2010-11-12 09:48:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
On Site Datetime
2010-11-12 10:02:00
Nrc Rpt Datetime
2010-11-12 11:03:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Pipe Fac Name
#6-12" Rosemount To Willmar Line
Segment Name
#6-12" Rosemount To Willmar Line
Onshore State Abbreviation
Mn
Onshore Postal Code
55378
Onshore City Name
Savage
Onshore County Name
Scott
Designated Location
Milepost/valve Station
Designated Name
9.2
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
72
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
12.75
Pipe Wall Thickness
0.25
Pipe Smys
52000
Pipe Specification
Api 5lx
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Installation Year
1954
Manufactured Year
1954
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Surface Water Remed Ind
Yes
Groundwater Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Groundwater Contam Ind
Yes
Amount Released
0.5
Rel Water Name
Storm Water Channel Inside Industrial Facility
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
500
Est Cost Prop Damage
33000
Est Cost Emergency
100000
Est Cost Environmental
260000
Est Cost Other
0
Prpty
393500
Accident Psig
920
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
24009
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Scada did not indicate any issues and this was classified as a low rate release which is undetectable in the control room.
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Material Failure Of Pipe Or Weld
Cause Details
Design-, Construction-, Installation-, Or Fabrication-Related
Metallurgical Ind
Yes
Failure Type
Design-, Construction-, Installation-, Or Fabrication-Related
Other Factor
Yes
Other Factor Details
Crack Located In Dent Caused By Rock At 5:00 Position In Pipe.
Additional Dent Ind
Yes
Collected Data Ind
Yes
Cir Trn Wave Mgn Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Circ Wave Recent Year
2007
Geometry Recent Year
2007
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
1992
Hydrtst Most Rcnt Pressure
1884
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
K****** L* L*******
Preparer Title
Senior Compliance Coordinator
Preparer Email
K***********@m*********.com
Preparer Telephone
918-574-7315
Preparer Fax
918-574-7246
Prepared Date
2011-04-01 00:00:00
Authorizer Name
K****** L* L*******
Authorizer Telephone
918-574-7315
Authorizer Title
Senior Compliance Coordinator
Authorizer Email
K***********@m*********.com
Narrative
Magellan's northern district office was notified of a reported sheen on water in a drainage ditch by the minnesota pollution control agency. The northern district office informed magellan's operations control center whereupon the line was immediately shut down. Up-and-down stream valves were closed and a ground search was conducted which included excavating the line in the vicinity of the reported sighting. A large rock was discovered immediately under the pipeline. When the rock was removed a leak was discovered on the bottom of the pipe which had been resting on the rock. Metallurgical analysis determined the cause of the release as a through the wall crack in a bottom side deformation anomaly that grew from mechanical damage on the inside surface of the pipe.
Report Received Date 2010-12-10 00:00:00
Iyear 2010
Report Number 20100290
Supplemental Number 15722
Report Type Supplemental Final
Operator Id 22610 PHMSA Enforcement
Name Magellan Pipeline Company, Lp
Operator Street Address 100 West 5th Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2010-11-12 09:48:00
Location Latitude 44.77328 Google Maps OpenStreetMap
Location Longitude -93.35844 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 48
Intentional Release Bbls 0
Recovered Bbls 48
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Minnesota Pollution Control Agency
Incident Identified Datetime 2010-11-12 09:48:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
On Site Datetime 2010-11-12 10:02:00
Nrc Rpt Datetime 2010-11-12 11:03:00
Nrc Rpt Num 959677 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Pipe Fac Name #6-12" Rosemount To Willmar Line
Segment Name #6-12" Rosemount To Willmar Line
Onshore State Abbreviation Mn
Onshore Postal Code 55378
Onshore City Name Savage
Onshore County Name Scott
Designated Location Milepost/valve Station
Designated Name 9.2
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 72
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 12.75
Pipe Wall Thickness 0.25
Pipe Smys 52000
Pipe Specification Api 5lx
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Installation Year 1954
Manufactured Year 1954
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Surface Water Remed Ind Yes
Groundwater Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Groundwater Contam Ind Yes
Amount Released 0.5
Rel Water Name Storm Water Channel Inside Industrial Facility
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 500
Est Cost Prop Damage 33000
Est Cost Emergency 100000
Est Cost Environmental 260000
Est Cost Other 0
Prpty 393500
Accident Psig 920
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 24009
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Scada did not indicate any issues and this was classified as a low rate release which is undetectable in the control room.
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 1
Num Employees Failed 0
Cause Material Failure Of Pipe Or Weld
Cause Details Design-, Construction-, Installation-, Or Fabrication-Related
Metallurgical Ind Yes
Failure Type Design-, Construction-, Installation-, Or Fabrication-Related
Other Factor Yes
Other Factor Details Crack Located In Dent Caused By Rock At 5:00 Position In Pipe.
Additional Dent Ind Yes
Collected Data Ind Yes
Cir Trn Wave Mgn Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Circ Wave Recent Year 2007
Geometry Recent Year 2007
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 1992
Hydrtst Most Rcnt Pressure 1884
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name K****** L* L*******
Preparer Title Senior Compliance Coordinator
Preparer Email K***********@m*********.com
Preparer Telephone 918-574-7315
Preparer Fax 918-574-7246
Prepared Date 2011-04-01 00:00:00
Authorizer Name K****** L* L*******
Authorizer Telephone 918-574-7315
Authorizer Title Senior Compliance Coordinator
Authorizer Email K***********@m*********.com
Narrative Magellan's northern district office was notified of a reported sheen on water in a drainage ditch by the minnesota pollution control agency. The northern district office informed magellan's operations control center whereupon the line was immediately shut down. Up-and-down stream valves were closed and a ground search was conducted which included excavating the line in the vicinity of the reported sighting. A large rock was discovered immediately under the pipeline. When the rock was removed a leak was discovered on the bottom of the pipe which had been resting on the rock. Metallurgical analysis determined the cause of the release as a through the wall crack in a bottom side deformation anomaly that grew from mechanical damage on the inside surface of the pipe.

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