HL incident on 2010-10-27 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$7,500
Incident datetime
2010-10-27 15:00
Report number
Location
TX
Narrative
Check valve on the sump pump discharge line failed causing the sump to overfill. Check valve on suction was replaced. 2nd check valve is being installed on line.
Detailed record list
Report Received Date
2010-12-07 00:00:00
Iyear
2010
Report Number
20100284
Supplemental Number
17473
Report Type
Supplemental Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2010-10-27 15:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
10
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Spill Was Contained In The Sump Area
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Pipe Fac Name
Hope Station
Segment Name
Sump Area
Onshore State Abbreviation
Tx
Onshore Postal Code
77995
Onshore City Name
Hope
Onshore County Name
Lavaca
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Sump
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
300
Est Cost Prop Damage
7500
Est Cost Emergency
0
Est Cost Environmental
20000
Est Cost Other
0
Prpty
27800
Accident Psig
0
Mop Psig
0
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
No
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The sump overfilled
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Check Valve Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
No Other Contributing Factors
Preparer Name
J**** P* S****
Preparer Title
Pipeline Compliance Specialist
Preparer Email
J******@e****.com
Preparer Telephone
7133813614
Preparer Fax
7133816811
Prepared Date
2013-03-12 00:00:00
Authorizer Name
J**** P* S****
Authorizer Telephone
7133813614
Authorizer Title
Pipeline Compliance Specialist
Authorizer Email
J******@e****.com
Narrative
Check valve on the sump pump discharge line failed causing the sump to overfill. Check valve on suction was replaced. 2nd check valve is being installed on line.
Report Received Date 2010-12-07 00:00:00
Iyear 2010
Report Number 20100284
Supplemental Number 17473
Report Type Supplemental Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2010-10-27 15:00:00
Location Latitude 29.19462 Google Maps OpenStreetMap
Location Longitude -96.98528 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 10
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Spill Was Contained In The Sump Area
Nrc Rpt Num 958230 NRC Report How to search
Ignite Ind No
Explode Ind No
Pipe Fac Name Hope Station
Segment Name Sump Area
Onshore State Abbreviation Tx
Onshore Postal Code 77995
Onshore City Name Hope
Onshore County Name Lavaca
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Sump
Material Involved Carbon Steel
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 300
Est Cost Prop Damage 7500
Est Cost Emergency 0
Est Cost Environmental 20000
Est Cost Other 0
Prpty 27800
Accident Psig 0
Mop Psig 0
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind No
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The sump overfilled
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Check Valve Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details No Other Contributing Factors
Preparer Name J**** P* S****
Preparer Title Pipeline Compliance Specialist
Preparer Email J******@e****.com
Preparer Telephone 7133813614
Preparer Fax 7133816811
Prepared Date 2013-03-12 00:00:00
Authorizer Name J**** P* S****
Authorizer Telephone 7133813614
Authorizer Title Pipeline Compliance Specialist
Authorizer Email J******@e****.com
Narrative Check valve on the sump pump discharge line failed causing the sump to overfill. Check valve on suction was replaced. 2nd check valve is being installed on line.

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