HL incident on 2010-11-15 — TX

Operator
Sunoco Pipeline L.p.
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$8,875
Incident datetime
2010-11-15 18:51
Report number
Location
TX
Narrative
The drain valve on the pig trap was left open thereby allowing an uncontrolled flow of oil into the sump via the drain line. At the same time the high-high level alarm on the sump failed causing the oil to overfill the sump.
Detailed record list
Report Received Date
2010-12-06 00:00:00
Iyear
2010
Report Number
20100282
Supplemental Number
15521
Report Type
Supplemental Final
Operator Id
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2010-11-15 18:51:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
15
Intentional Release Bbls
0
Recovered Bbls
10
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2010-11-15 18:51:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Station Was Down At The Time
On Site Datetime
2010-11-15 18:51:00
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Check Valve
Pipe Fac Name
Diboll Station
Segment Name
Etx 10"
Onshore State Abbreviation
Tx
Onshore Postal Code
75941
Onshore City Name
Diboll
Onshore County Name
Angeline
Designated Location
Survey Station No.
Designated Name
5228+54
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Transition Area
Incident Area Subtype
Soil/air Interface
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Scraper/pig Trap
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
405
Est Cost Prop Damage
8875
Est Cost Emergency
5589
Est Cost Environmental
4565
Est Cost Other
0
Prpty
19434
Accident Psig
0
Mop Psig
1000
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
150
Internal Inspection Ind
No
Other Inspection Ind
Yes
Internal Inspection Details
Sump Drain Line
Operation Complications Ind
Yes
Other Complications Ind
Yes
Inspect Comp Details
Small Diameter Drain Line
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
No
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
No
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Because it was an instrumental error.
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
Yes
Num Employees Tested
1
Num Employees Failed
0
Num Contractors Tested
1
Num Contractors Failed
0
Cause
Incorrect Operation
Cause Details
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind
Valve Misalignment
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
K****** D**** B***
Preparer Title
Area Dot Compliance Supervisor
Preparer Email
K*****@s**************.com
Preparer Telephone
281-637-6497
Preparer Fax
281-637-6425
Prepared Date
2011-01-11 00:00:00
Authorizer Name
K****** D**** B***
Authorizer Telephone
281-637-6497
Authorizer Title
Area Dot Compliance Supervisor
Authorizer Email
K*****@s**************.com
Narrative
The drain valve on the pig trap was left open thereby allowing an uncontrolled flow of oil into the sump via the drain line. At the same time the high-high level alarm on the sump failed causing the oil to overfill the sump.
Report Received Date 2010-12-06 00:00:00
Iyear 2010
Report Number 20100282
Supplemental Number 15521
Report Type Supplemental Final
Operator Id 18718 PHMSA Enforcement
Name Sunoco Pipeline L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2010-11-15 18:51:00
Location Latitude 31.1591 Google Maps OpenStreetMap
Location Longitude -94.6759 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 15
Intentional Release Bbls 0
Recovered Bbls 10
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2010-11-15 18:51:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Station Was Down At The Time
On Site Datetime 2010-11-15 18:51:00
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Check Valve
Pipe Fac Name Diboll Station
Segment Name Etx 10"
Onshore State Abbreviation Tx
Onshore Postal Code 75941
Onshore City Name Diboll
Onshore County Name Angeline
Designated Location Survey Station No.
Designated Name 5228+54
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Transition Area
Incident Area Subtype Soil/air Interface
Crossing No
Pipe Facility Type Intrastate
Item Involved Scraper/pig Trap
Material Involved Carbon Steel
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 405
Est Cost Prop Damage 8875
Est Cost Emergency 5589
Est Cost Environmental 4565
Est Cost Other 0
Prpty 19434
Accident Psig 0
Mop Psig 1000
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 150
Internal Inspection Ind No
Other Inspection Ind Yes
Internal Inspection Details Sump Drain Line
Operation Complications Ind Yes
Other Complications Ind Yes
Inspect Comp Details Small Diameter Drain Line
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind No
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind No
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Because it was an instrumental error.
Employee Drug Test Ind Yes
Contractor Drug Test Ind Yes
Num Employees Tested 1
Num Employees Failed 0
Num Contractors Tested 1
Num Contractors Failed 0
Cause Incorrect Operation
Cause Details Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind Valve Misalignment
Related Failure Follow Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name K****** D**** B***
Preparer Title Area Dot Compliance Supervisor
Preparer Email K*****@s**************.com
Preparer Telephone 281-637-6497
Preparer Fax 281-637-6425
Prepared Date 2011-01-11 00:00:00
Authorizer Name K****** D**** B***
Authorizer Telephone 281-637-6497
Authorizer Title Area Dot Compliance Supervisor
Authorizer Email K*****@s**************.com
Narrative The drain valve on the pig trap was left open thereby allowing an uncontrolled flow of oil into the sump via the drain line. At the same time the high-high level alarm on the sump failed causing the oil to overfill the sump.

All rights reserved. Copyright © by ClearPHMSA