HL incident on 2010-10-21 — TX

Operator
Kinder Morgan Co2 Co. Lp
Cause
Other Accident Cause
Commodity
Co2 (Carbon Dioxide)
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$600
Incident datetime
2010-10-21 17:24
Report number
Location
TX
Narrative
On 10/21/2010 at 17:26 at km CO2 mccamey station located in upton county, a relief valve set and calibrated to operate at 2160 psi popped/vented to atmosphere at 2085 psig due to a pressure surge from third party pump facility. The relief duration was from 17:26 until 19:16 at 2030 psi average pressure. The relief valve is installed in a location to protect kinder morgan's pipeline. However, the initial set point was set too low for the established mop of the line. The set point has been reset to 105% of the mop, 2330 psig.
Detailed record list
Report Received Date
2010-11-19 00:00:00
Iyear
2010
Report Number
20100247
Supplemental Number
17830
Report Type
Supplemental Final
Operator Id
Name
Kinder Morgan Co2 Co. Lp
Operator Street Address
1001 Louisiana Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2010-10-21 17:24:00
Location Latitude
Location Longitude
Commodity Released Type
Co2 (Carbon Dioxide)
Unintentional Release Bbls
299
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Ignite Ind
No
Explode Ind
No
Onshore State Abbreviation
Tx
Onshore Postal Code
79752
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Relief Valve
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Pressure Surge
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
675
Est Cost Prop Damage
600
Est Cost Emergency
250
Est Cost Environmental
0
Est Cost Other
0
Prpty
1525
Accident Psig
2085
Mop Psig
2220
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Pressure spike caused by third party operated pump surge
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Accident Cause
Cause Details
Miscellaneous
Other Type
Miscellaneous
Misc Details
Pressure Surge From Third Party Operator And Lack Of Communication; Kinder Morgan's Relief Valve Set Point Was Set Too Low
Preparer Name
A**** Z*****
Preparer Title
Regulatory Compliance Manager
Preparer Email
A***********@k***********.com
Preparer Telephone
7133699512
Preparer Fax
3039843417
Prepared Date
2013-04-05 00:00:00
Authorizer Name
J*** J***** J****
Authorizer Telephone
7133699721
Authorizer Title
Director Of Transportation
Authorizer Email
J*********@k***********.com
Narrative
On 10/21/2010 at 17:26 at km CO2 mccamey station located in upton county, a relief valve set and calibrated to operate at 2160 psi popped/vented to atmosphere at 2085 psig due to a pressure surge from third party pump facility. The relief duration was from 17:26 until 19:16 at 2030 psi average pressure. The relief valve is installed in a location to protect kinder morgan's pipeline. However, the initial set point was set too low for the established mop of the line. The set point has been reset to 105% of the mop, 2330 psig.
Report Received Date 2010-11-19 00:00:00
Iyear 2010
Report Number 20100247
Supplemental Number 17830
Report Type Supplemental Final
Operator Id 31555 PHMSA Enforcement
Name Kinder Morgan Co2 Co. Lp
Operator Street Address 1001 Louisiana Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2010-10-21 17:24:00
Location Latitude 31.06576 Google Maps OpenStreetMap
Location Longitude -103.17361 Google Maps OpenStreetMap
Commodity Released Type Co2 (Carbon Dioxide)
Unintentional Release Bbls 299
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Ignite Ind No
Explode Ind No
Onshore State Abbreviation Tx
Onshore Postal Code 79752
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Relief Valve
Material Involved Carbon Steel
Release Type Other
Release Type Details Pressure Surge
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 675
Est Cost Prop Damage 600
Est Cost Emergency 250
Est Cost Environmental 0
Est Cost Other 0
Prpty 1525
Accident Psig 2085
Mop Psig 2220
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Pressure spike caused by third party operated pump surge
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Accident Cause
Cause Details Miscellaneous
Other Type Miscellaneous
Misc Details Pressure Surge From Third Party Operator And Lack Of Communication; Kinder Morgan's Relief Valve Set Point Was Set Too Low
Preparer Name A**** Z*****
Preparer Title Regulatory Compliance Manager
Preparer Email A***********@k***********.com
Preparer Telephone 7133699512
Preparer Fax 3039843417
Prepared Date 2013-04-05 00:00:00
Authorizer Name J*** J***** J****
Authorizer Telephone 7133699721
Authorizer Title Director Of Transportation
Authorizer Email J*********@k***********.com
Narrative On 10/21/2010 at 17:26 at km CO2 mccamey station located in upton county, a relief valve set and calibrated to operate at 2160 psi popped/vented to atmosphere at 2085 psig due to a pressure surge from third party pump facility. The relief duration was from 17:26 until 19:16 at 2030 psi average pressure. The relief valve is installed in a location to protect kinder morgan's pipeline. However, the initial set point was set too low for the established mop of the line. The set point has been reset to 105% of the mop, 2330 psig.

All rights reserved. Copyright © by ClearPHMSA