HL incident on 2010-11-05 — OK

Operator
Oneok Ngl Pipeline Lp
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$10
Incident datetime
2010-11-05 11:00
Report number
Location
OK
Narrative
Third party was waiting to enter site noticed ice ball on valve, contacted field personnel. Field personnel arrived on site installed threaded plug in weep hole of valve stopping leak.
Detailed record list
Report Received Date
2010-11-18 00:00:00
Iyear
2010
Report Number
20100245
Supplemental Number
15376
Report Type
Original Final
Operator Id
Name
Oneok Ngl Pipeline Lp
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2010-11-05 08:00:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
3.53
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2010-11-05 11:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Body Of Valve Blew Down And Installed Plug In Weep Hole Of Valve
On Site Datetime
2010-11-05 11:35:00
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
10026/criner Station
Segment Name
10026
Onshore State Abbreviation
Ok
Onshore Postal Code
73080
Onshore City Name
Purcell
Onshore County Name
Mcclain
Designated Location
Milepost/valve Station
Designated Name
7162+05
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Gate
Valve Manufacturer
M & J
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Gas Released
149
Est Cost Prop Damage
10
Prpty
159
Accident Psig
600
Mop Psig
1203
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Gathering
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind
Yes
Eq Additional Other Details
Wear
Preparer Name
P**** G**********
Preparer Email
P****************@o****.com
Preparer Telephone
580-395-6238
Preparer Fax
580-395-2933
Prepared Date
2010-11-17 00:00:00
Authorizer Name
N*** J****
Authorizer Telephone
580-395-6304
Authorizer Email
N*********@o****.com
Narrative
Third party was waiting to enter site noticed ice ball on valve, contacted field personnel. Field personnel arrived on site installed threaded plug in weep hole of valve stopping leak.
Report Received Date 2010-11-18 00:00:00
Iyear 2010
Report Number 20100245
Supplemental Number 15376
Report Type Original Final
Operator Id 32109 PHMSA Enforcement
Name Oneok Ngl Pipeline Lp
Operator Street Address 100 West Fifth Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2010-11-05 08:00:00
Location Latitude 34.94418 Google Maps OpenStreetMap
Location Longitude -97.47736 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 3.53
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2010-11-05 11:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Body Of Valve Blew Down And Installed Plug In Weep Hole Of Valve
On Site Datetime 2010-11-05 11:35:00
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name 10026/criner Station
Segment Name 10026
Onshore State Abbreviation Ok
Onshore Postal Code 73080
Onshore City Name Purcell
Onshore County Name Mcclain
Designated Location Milepost/valve Station
Designated Name 7162+05
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Gate
Valve Manufacturer M & J
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Gas Released 149
Est Cost Prop Damage 10
Prpty 159
Accident Psig 600
Mop Psig 1203
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Gathering
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind Yes
Eq Additional Other Details Wear
Preparer Name P**** G**********
Preparer Email P****************@o****.com
Preparer Telephone 580-395-6238
Preparer Fax 580-395-2933
Prepared Date 2010-11-17 00:00:00
Authorizer Name N*** J****
Authorizer Telephone 580-395-6304
Authorizer Email N*********@o****.com
Narrative Third party was waiting to enter site noticed ice ball on valve, contacted field personnel. Field personnel arrived on site installed threaded plug in weep hole of valve stopping leak.

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