HL incident on 2010-02-04 — PA

Operator
West Shore Pipeline Co
Cause
Natural Force Damage
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,500
Incident datetime
2010-02-04 15:10
Report number
Location
PA
Narrative
At 3:10 pm on february 4, 2010, a release was identified by west shore personnel at the mitchell field terminal. The line was not running at the time. The line was isolated and emergency response procedures were initiated. 10 gallons of jet fuel leaked through a pipe nipple connected to the prover. The cause of the release has been determined to be frost heave causing fatigue in the thread area of the pipe fitting, in addition to the absence of an expansion joint. Repairs were made and the line is back in service. All remediation is complete. No further action is required. Supplemental/final report filed to populate field e5.F
Detailed record list
Report Received Date
2010-11-17 00:00:00
Iyear
2010
Report Number
20100244
Supplemental Number
17856
Report Type
Supplemental Final
Operator Id
Name
West Shore Pipeline Co
Operator Street Address
5 Tek Park
Operator City Name
Breinigsville
Operator State Abbreviation
PA
Operator Postal Code
18031
Local Datetime
2010-02-04 15:10:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
0.24
Intentional Release Bbls
0
Recovered Bbls
0.19
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Ignite Ind
No
Explode Ind
No
Pipe Fac Name
Mitchell Field Terminal
Segment Name
Mf
Onshore State Abbreviation
Wi
Onshore Postal Code
53154
Onshore City Name
Milwaukee
Onshore County Name
Milwaukee
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Pipe Facility Type
Interstate
Item Involved
Instrumentation
Release Type
Leak
Leak Type
Crack
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
35
Est Cost Prop Damage
2500
Est Cost Emergency
0
Est Cost Environmental
1986
Est Cost Other
0
Prpty
4521
Pipeline Function
< 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Natural Force Damage
Cause Details
Temperature
Natural Force Type
Temperature
Nf Extreme Weather Ind
No
Preparer Name
J*** B R*******
Preparer Title
Compliance Manager
Preparer Email
J********@b******.com
Preparer Telephone
610.904.4185
Preparer Fax
610.904.4545
Prepared Date
2013-04-09 00:00:00
Authorizer Name
J*** R*******
Authorizer Telephone
610-904-4185
Authorizer Title
Compliance Manager
Authorizer Email
J********@b******.com
Narrative
At 3:10 pm on february 4, 2010, a release was identified by west shore personnel at the mitchell field terminal. The line was not running at the time. The line was isolated and emergency response procedures were initiated. 10 gallons of jet fuel leaked through a pipe nipple connected to the prover. The cause of the release has been determined to be frost heave causing fatigue in the thread area of the pipe fitting, in addition to the absence of an expansion joint. Repairs were made and the line is back in service. All remediation is complete. No further action is required. Supplemental/final report filed to populate field e5.F
Report Received Date 2010-11-17 00:00:00
Iyear 2010
Report Number 20100244
Supplemental Number 17856
Report Type Supplemental Final
Operator Id 22430 PHMSA Enforcement
Name West Shore Pipeline Co
Operator Street Address 5 Tek Park
Operator City Name Breinigsville
Operator State Abbreviation PA
Operator Postal Code 18031
Local Datetime 2010-02-04 15:10:00
Location Latitude 42.9289 Google Maps OpenStreetMap
Location Longitude -87.8884 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 0.24
Intentional Release Bbls 0
Recovered Bbls 0.19
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Ignite Ind No
Explode Ind No
Pipe Fac Name Mitchell Field Terminal
Segment Name Mf
Onshore State Abbreviation Wi
Onshore Postal Code 53154
Onshore City Name Milwaukee
Onshore County Name Milwaukee
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Pipe Facility Type Interstate
Item Involved Instrumentation
Release Type Leak
Leak Type Crack
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 35
Est Cost Prop Damage 2500
Est Cost Emergency 0
Est Cost Environmental 1986
Est Cost Other 0
Prpty 4521
Pipeline Function < 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Natural Force Damage
Cause Details Temperature
Natural Force Type Temperature
Nf Extreme Weather Ind No
Preparer Name J*** B R*******
Preparer Title Compliance Manager
Preparer Email J********@b******.com
Preparer Telephone 610.904.4185
Preparer Fax 610.904.4545
Prepared Date 2013-04-09 00:00:00
Authorizer Name J*** R*******
Authorizer Telephone 610-904-4185
Authorizer Title Compliance Manager
Authorizer Email J********@b******.com
Narrative At 3:10 pm on february 4, 2010, a release was identified by west shore personnel at the mitchell field terminal. The line was not running at the time. The line was isolated and emergency response procedures were initiated. 10 gallons of jet fuel leaked through a pipe nipple connected to the prover. The cause of the release has been determined to be frost heave causing fatigue in the thread area of the pipe fitting, in addition to the absence of an expansion joint. Repairs were made and the line is back in service. All remediation is complete. No further action is required. Supplemental/final report filed to populate field e5.F

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