HL incident on 2010-01-11 — KS

Operator
Jayhawk Pipeline Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,000
Incident datetime
2010-01-11 15:00
Report number
Location
KS
Narrative
Company personnel while doing station inspections found small amount of oil coming up around suction pipe to an idled pump inside of pump building with concrete floor. Line was shut down and isolated. Portions of concrete floor were cut out and removed and soil was removed around suction line to find small pinhole leak in elbow at bottom of suction pipe. Line was rerouted so that it no longer was underneath pumphouse floor and line was put back into service. This report was initially filed as a hard copy because electronic version of new form was not ready for use.I was then asked by PHMSA to fill out electronically several months later
Detailed record list
Report Received Date
2010-10-22 00:00:00
Iyear
2010
Report Number
20100234
Supplemental Number
18134
Report Type
Supplemental Final
Operator Id
Name
Jayhawk Pipeline Llc
Operator Street Address
2000 South Main
Operator City Name
Mcpherson
Operator State Abbreviation
KS
Operator Postal Code
67460
Local Datetime
2010-01-11 15:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2010-01-11 15:00:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2010-01-11 15:10:00
Restart Datetime
2010-01-13 14:00:00
On Site Datetime
2010-01-11 15:05:00
Ignite Ind
No
Explode Ind
No
Pipe Fac Name
Chase Kaw Terminal
Segment Name
Chase To Lyons 8"
Onshore State Abbreviation
Ks
Onshore Postal Code
67524
Onshore City Name
Chase
Onshore County Name
Rice
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under A Building
Pipe Facility Type
Intrastate
Item Involved
Other
Item Involved Details
Elbow
Release Type
Leak
Leak Type
Pinhole
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
150
Est Cost Prop Damage
2000
Est Cost Emergency
3000
Est Cost Environmental
6500
Est Cost Other
500
Est Cost Other Details
Vac Truck
Prpty
12150
Pipeline Function
< 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Preparer Name
D**** A* C***
Preparer Title
Manager Of Operations
Preparer Email
D****@j********.com
Preparer Telephone
620-241-9260
Preparer Fax
620-241-9260
Prepared Date
2013-05-29 00:00:00
Authorizer Name
D**** A* C***
Authorizer Telephone
620.241.9260
Authorizer Title
Manager Of Operation
Authorizer Email
D****@j********.com
Narrative
Company personnel while doing station inspections found small amount of oil coming up around suction pipe to an idled pump inside of pump building with concrete floor. Line was shut down and isolated. Portions of concrete floor were cut out and removed and soil was removed around suction line to find small pinhole leak in elbow at bottom of suction pipe. Line was rerouted so that it no longer was underneath pumphouse floor and line was put back into service. This report was initially filed as a hard copy because electronic version of new form was not ready for use.I was then asked by PHMSA to fill out electronically several months later
Report Received Date 2010-10-22 00:00:00
Iyear 2010
Report Number 20100234
Supplemental Number 18134
Report Type Supplemental Final
Operator Id 9175 PHMSA Enforcement
Name Jayhawk Pipeline Llc
Operator Street Address 2000 South Main
Operator City Name Mcpherson
Operator State Abbreviation KS
Operator Postal Code 67460
Local Datetime 2010-01-11 15:00:00
Location Latitude 38.34519 Google Maps OpenStreetMap
Location Longitude -98.31356 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2
Recovered Bbls 1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2010-01-11 15:00:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2010-01-11 15:10:00
Restart Datetime 2010-01-13 14:00:00
On Site Datetime 2010-01-11 15:05:00
Ignite Ind No
Explode Ind No
Pipe Fac Name Chase Kaw Terminal
Segment Name Chase To Lyons 8"
Onshore State Abbreviation Ks
Onshore Postal Code 67524
Onshore City Name Chase
Onshore County Name Rice
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under A Building
Pipe Facility Type Intrastate
Item Involved Other
Item Involved Details Elbow
Release Type Leak
Leak Type Pinhole
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 150
Est Cost Prop Damage 2000
Est Cost Emergency 3000
Est Cost Environmental 6500
Est Cost Other 500
Est Cost Other Details Vac Truck
Prpty 12150
Pipeline Function < 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Preparer Name D**** A* C***
Preparer Title Manager Of Operations
Preparer Email D****@j********.com
Preparer Telephone 620-241-9260
Preparer Fax 620-241-9260
Prepared Date 2013-05-29 00:00:00
Authorizer Name D**** A* C***
Authorizer Telephone 620.241.9260
Authorizer Title Manager Of Operation
Authorizer Email D****@j********.com
Narrative Company personnel while doing station inspections found small amount of oil coming up around suction pipe to an idled pump inside of pump building with concrete floor. Line was shut down and isolated. Portions of concrete floor were cut out and removed and soil was removed around suction line to find small pinhole leak in elbow at bottom of suction pipe. Line was rerouted so that it no longer was underneath pumphouse floor and line was put back into service. This report was initially filed as a hard copy because electronic version of new form was not ready for use.I was then asked by PHMSA to fill out electronically several months later

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