HL incident on 2010-09-08 — OK

Operator
Oneok Ngl Pipeline Lp
Cause
Incorrect Operation
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2010-09-08 16:22
Report number
Location
OK
Narrative
A pipeline delivery was being set-up in preparation for a movement on the 100 pipeline. Due to a communication error, the product flow was unknowingly diverted to a blocked in section of pipeline resulting in a pressures rise, although not in excess of operating limit. A thermal relief valve opened at 746 psi for 1 minute resulting in approximately 0.85 barrels of liquid vented to the air. No indication of any liquid hitting the ground. Because of the above mentioned closed valve there was 2 separate locations where thermal relief valves opened. The other report that is related to this incident is 20100218.
Detailed record list
Report Received Date
2010-10-06 00:00:00
Iyear
2010
Report Number
20100217
Supplemental Number
17311
Report Type
Supplemental Final
Operator Id
Name
Oneok Ngl Pipeline Lp
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2010-09-08 16:22:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Natural Gasoline
Unintentional Release Bbls
0.85
Intentional Release Bbls
0.1
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Controller
Operator Type
Operator Employee
Incident Identified Datetime
2010-09-08 16:22:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
On Site Datetime
2010-09-08 16:22:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
212 Meter Run At Conway Storage
Segment Name
11313
Onshore State Abbreviation
Ks
Onshore Postal Code
67491
Onshore City Name
Windom
Onshore County Name
Mcpherson
Designated Location
Milepost/valve Station
Designated Name
Site 421
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Relief Valve
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Thermal Relief Valve Relieved To Atmosphere
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
60
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
60
Accident Psig
746.5
Mop Psig
692
Accident Pressure
Pressure Exceeded Mop, But Did Not Exceed 110% Of Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Schedule Ind
Yes
Invest No Schedule Ind Details
Root Casue Determined This Was Not A Factor
Invest Incorrect Action Ind
Yes
Invest Incorrect Procedure Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Pipeline Or Equipment Overpressured
Operation Type
Pipeline Or Equipment Overpressured
Related Failure Follow Ind
Yes
Category Type
Normal Operating Conditions
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
P**** G**********
Preparer Email
P****************@o****.com
Preparer Telephone
580-395-6238
Preparer Fax
580-395-2933
Prepared Date
2013-03-04 00:00:00
Authorizer Name
N*** J****
Authorizer Telephone
580-395-6304
Authorizer Email
N*********@o****.com
Narrative
A pipeline delivery was being set-up in preparation for a movement on the 100 pipeline. Due to a communication error, the product flow was unknowingly diverted to a blocked in section of pipeline resulting in a pressures rise, although not in excess of operating limit. A thermal relief valve opened at 746 psi for 1 minute resulting in approximately 0.85 barrels of liquid vented to the air. No indication of any liquid hitting the ground. Because of the above mentioned closed valve there was 2 separate locations where thermal relief valves opened. The other report that is related to this incident is 20100218.
Report Received Date 2010-10-06 00:00:00
Iyear 2010
Report Number 20100217
Supplemental Number 17311
Report Type Supplemental Final
Operator Id 32109 PHMSA Enforcement
Name Oneok Ngl Pipeline Lp
Operator Street Address 100 West Fifth Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2010-09-08 16:22:00
Location Latitude 38.37239 Google Maps OpenStreetMap
Location Longitude -97.80143 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Natural Gasoline
Unintentional Release Bbls 0.85
Intentional Release Bbls 0.1
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Controller
Operator Type Operator Employee
Incident Identified Datetime 2010-09-08 16:22:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
On Site Datetime 2010-09-08 16:22:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name 212 Meter Run At Conway Storage
Segment Name 11313
Onshore State Abbreviation Ks
Onshore Postal Code 67491
Onshore City Name Windom
Onshore County Name Mcpherson
Designated Location Milepost/valve Station
Designated Name Site 421
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Relief Valve
Material Involved Carbon Steel
Release Type Other
Release Type Details Thermal Relief Valve Relieved To Atmosphere
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 60
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 60
Accident Psig 746.5
Mop Psig 692
Accident Pressure Pressure Exceeded Mop, But Did Not Exceed 110% Of Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Schedule Ind Yes
Invest No Schedule Ind Details Root Casue Determined This Was Not A Factor
Invest Incorrect Action Ind Yes
Invest Incorrect Procedure Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Pipeline Or Equipment Overpressured
Operation Type Pipeline Or Equipment Overpressured
Related Failure Follow Ind Yes
Category Type Normal Operating Conditions
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name P**** G**********
Preparer Email P****************@o****.com
Preparer Telephone 580-395-6238
Preparer Fax 580-395-2933
Prepared Date 2013-03-04 00:00:00
Authorizer Name N*** J****
Authorizer Telephone 580-395-6304
Authorizer Email N*********@o****.com
Narrative A pipeline delivery was being set-up in preparation for a movement on the 100 pipeline. Due to a communication error, the product flow was unknowingly diverted to a blocked in section of pipeline resulting in a pressures rise, although not in excess of operating limit. A thermal relief valve opened at 746 psi for 1 minute resulting in approximately 0.85 barrels of liquid vented to the air. No indication of any liquid hitting the ground. Because of the above mentioned closed valve there was 2 separate locations where thermal relief valves opened. The other report that is related to this incident is 20100218.

All rights reserved. Copyright © by ClearPHMSA