Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2010-08-20 — OK
Operator
Magellan Terminals Holdings, Lp
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
—
Incident datetime
2010-08-20 07:00
Report number
Location
OK
Narrative
A sample drain valve was found open at the pc4 valve site. Product had migrated to the valve site box.
Detailed record list
Report Received Date
2010-09-17 00:00:00
Iyear
2010
Report Number
20100202
Supplemental Number
15297
Report Type
Original
Operator Id
31580
Name
Magellan Terminals Holdings, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2010-08-20 07:00:00
Location Latitude
29.718312
Location Longitude
-95.180385
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
14
Intentional Release Bbls
0
Recovered Bbls
14
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2010-08-20 07:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Sample Drain Valve; Idle Line
On Site Datetime
2010-08-20 07:15:00
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Galena Park Terminal
Segment Name
Pc4 Valve Site
Onshore State Abbreviation
Tx
Onshore Postal Code
77501
Onshore City Name
Pasedena
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Other
Item Involved Details
Sample Drain Valve
Installation Year
2000
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Operator Error
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Emergency
5000
Est Cost Environmental
15000
Prpty
20000
Accident Psig
60
Mop Psig
540
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
20
Internal Inspection Ind
No
Tight Mitered Ind
Yes
Operation Complications Ind
Yes
Other Complications Ind
Yes
Inspect Comp Details
Sample Drain Valve
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Related Failure Follow Ind
Yes
Category Type
Normal Operating Conditions
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
D******* C*********
Preparer Title
Compliance Coordinator Sr
Preparer Email
D******************@m*********.com
Preparer Telephone
9185747386
Preparer Fax
9185747246
Prepared Date
2010-09-15 00:00:00
Authorizer Name
D******* C*********
Authorizer Telephone
9185747386
Authorizer Title
Compliance Coordinator Sr
Authorizer Email
D******************@m*********.com
Narrative
A sample drain valve was found open at the pc4 valve site. Product had migrated to the valve site box.
| Report Received Date | 2010-09-17 00:00:00 |
|---|---|
| Iyear | 2010 |
| Report Number | 20100202 |
| Supplemental Number | 15297 |
| Report Type | Original |
| Operator Id | 31580 PHMSA Enforcement |
| Name | Magellan Terminals Holdings, Lp |
| Operator Street Address | 100 West 5th Street |
| Operator City Name | Tulsa |
| Operator State Abbreviation | OK |
| Operator Postal Code | 74103 |
| Local Datetime | 2010-08-20 07:00:00 |
| Location Latitude | 29.718312 Google Maps OpenStreetMap |
| Location Longitude | -95.180385 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Diesel, Fuel Oil, Kerosene, Jet Fuel |
| Unintentional Release Bbls | 14 |
| Intentional Release Bbls | 0 |
| Recovered Bbls | 14 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Local Operating Personnel, Including Contractors |
| Operator Type | Operator Employee |
| Incident Identified Datetime | 2010-08-20 07:00:00 |
| System Part Involved | Onshore Pipeline, Including Valve Sites |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | Sample Drain Valve; Idle Line |
| On Site Datetime | 2010-08-20 07:15:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Upstream Valve Type Ind | Manual |
| Downstream Valve Type Ind | Manual |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Galena Park Terminal |
| Segment Name | Pc4 Valve Site |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 77501 |
| Onshore City Name | Pasedena |
| Onshore County Name | Harris |
| Designated Location | Milepost/valve Station |
| Designated Name | 0 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
| Crossing | No |
| Pipe Facility Type | Intrastate |
| Item Involved | Other |
| Item Involved Details | Sample Drain Valve |
| Installation Year | 2000 |
| Material Involved | Carbon Steel |
| Release Type | Other |
| Release Type Details | Operator Error |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | Yes |
| Soil Remed Ind | Yes |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| Other Pop Ind | Yes |
| Other Pop Yes No | Yes |
| Est Cost Emergency | 5000 |
| Est Cost Environmental | 15000 |
| Prpty | 20000 |
| Accident Psig | 60 |
| Mop Psig | 540 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Length Segment Isolated | 20 |
| Internal Inspection Ind | No |
| Tight Mitered Ind | Yes |
| Operation Complications Ind | Yes |
| Other Complications Ind | Yes |
| Inspect Comp Details | Sample Drain Valve |
| Pipeline Function | < 20% Smys Regulated Transmission |
| Scada In Place Ind | No |
| Cpm In Place Ind | No |
| Investigation Status | No, the facility was not monitored by a controller(s) at the time of the accident |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Incorrect Operation |
| Cause Details | Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure |
| Operation Type | Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure |
| Related Failure Follow Ind | Yes |
| Category Type | Normal Operating Conditions |
| Operator Qualification Ind | Yes |
| Qualified Individuals | Yes, They Were Qualified For The Task(S) |
| Preparer Name | D******* C********* |
| Preparer Title | Compliance Coordinator Sr |
| Preparer Email | D******************@m*********.com |
| Preparer Telephone | 9185747386 |
| Preparer Fax | 9185747246 |
| Prepared Date | 2010-09-15 00:00:00 |
| Authorizer Name | D******* C********* |
| Authorizer Telephone | 9185747386 |
| Authorizer Title | Compliance Coordinator Sr |
| Authorizer Email | D******************@m*********.com |
| Narrative | A sample drain valve was found open at the pc4 valve site. Product had migrated to the valve site box. |
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