HL incident on 2010-08-19 — TX

Operator
Tc Oil Pipeline Operations Inc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2010-08-19 08:30
Report number
Location
TX
Narrative
The 1/2" check valve stuck open on the pressure transmitter on the suction side of the pump resulting in a release of crude oil through the ralston test port. The threaded dust cap on the check valve was not installed at the time of release. Site remediation completed.
Detailed record list
Report Received Date
2010-09-16 00:00:00
Iyear
2010
Report Number
20100200
Supplemental Number
17789
Report Type
Supplemental Final
Operator Id
Name
Tc Oil Pipeline Operations Inc
Operator Street Address
920 Memorial City Way Suite 800
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77024
Local Datetime
2010-08-19 08:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.24
Intentional Release Bbls
0
Recovered Bbls
0.24
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2010-08-19 08:30:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pump Station Off Line During Release.
On Site Datetime
2010-08-19 08:30:00
Nrc Rpt Datetime
2010-08-19 12:30:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Hartington Pump Station
Segment Name
Glacial Lakes
Onshore State Abbreviation
Ne
Onshore Postal Code
68739
Onshore City Name
Hartington
Onshore County Name
Cedar
Designated Location
Milepost/valve Station
Designated Name
454.9
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Instrumentation
Installation Year
2009
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
18
Est Cost Prop Damage
0
Est Cost Emergency
5000
Est Cost Environmental
28000
Est Cost Other
0
Prpty
33018
Accident Psig
500
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The pump station was off line at the time of the release and the cpm leak detection system was inactive. The oil conrol center controllers did not have ermote control of the pump and did not contribute to the release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Check Valve Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Debris In The Check Valve
Preparer Name
D***** C*******
Preparer Title
Regulatory Compliance Specialist
Preparer Email
D***********@t**********.com
Preparer Telephone
7012901176
Preparer Fax
7014831431
Prepared Date
2013-04-03 00:00:00
Authorizer Name
D***** C*******
Authorizer Telephone
7014831434
Authorizer Title
Regulatory Compiance Specialist
Authorizer Email
D***********@t**********.com
Narrative
The 1/2" check valve stuck open on the pressure transmitter on the suction side of the pump resulting in a release of crude oil through the ralston test port. The threaded dust cap on the check valve was not installed at the time of release. Site remediation completed.
Report Received Date 2010-09-16 00:00:00
Iyear 2010
Report Number 20100200
Supplemental Number 17789
Report Type Supplemental Final
Operator Id 32334 PHMSA Enforcement
Name Tc Oil Pipeline Operations Inc
Operator Street Address 920 Memorial City Way Suite 800
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77024
Local Datetime 2010-08-19 08:30:00
Location Latitude 42.63521 Google Maps OpenStreetMap
Location Longitude -97.3371 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.24
Intentional Release Bbls 0
Recovered Bbls 0.24
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2010-08-19 08:30:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Pump Station Off Line During Release.
On Site Datetime 2010-08-19 08:30:00
Nrc Rpt Datetime 2010-08-19 12:30:00
Nrc Rpt Num 951480 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Hartington Pump Station
Segment Name Glacial Lakes
Onshore State Abbreviation Ne
Onshore Postal Code 68739
Onshore City Name Hartington
Onshore County Name Cedar
Designated Location Milepost/valve Station
Designated Name 454.9
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Instrumentation
Installation Year 2009
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 18
Est Cost Prop Damage 0
Est Cost Emergency 5000
Est Cost Environmental 28000
Est Cost Other 0
Prpty 33018
Accident Psig 500
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The pump station was off line at the time of the release and the cpm leak detection system was inactive. The oil conrol center controllers did not have ermote control of the pump and did not contribute to the release.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Check Valve Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Debris In The Check Valve
Preparer Name D***** C*******
Preparer Title Regulatory Compliance Specialist
Preparer Email D***********@t**********.com
Preparer Telephone 7012901176
Preparer Fax 7014831431
Prepared Date 2013-04-03 00:00:00
Authorizer Name D***** C*******
Authorizer Telephone 7014831434
Authorizer Title Regulatory Compiance Specialist
Authorizer Email D***********@t**********.com
Narrative The 1/2" check valve stuck open on the pressure transmitter on the suction side of the pump resulting in a release of crude oil through the ralston test port. The threaded dust cap on the check valve was not installed at the time of release. Site remediation completed.

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