HL incident on 2010-08-12 — IL

Operator
Bp Pipeline (North America) Inc.
Cause
Material Failure Of Pipe Or Weld
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$220,000
Incident datetime
2010-08-12 17:00
Report number
Location
IL
Narrative
On 8-12-10, during the period between 1645 hrs and 1700 hrs, bp personnel responded to a 3rd party notification of hydrocarbon odors on/near bp's right of way, laporte, texas. Following initial assessment of the potential release site, bp generated an emergency one call, cleared the one-calls and began excavation on the bp-operated propylene pipeline at approximately 1930 hrs. The excavation site was continuously monitored for safe working atmospheric conditions. At approximately 2130 hrs the excavation was completed and the source was confirmed as bp's propylene line. At approximately 2245 hrs the leak was repaired with the installation of a plidco clamp. On 8-13-10 the pipeline was inspected and recoated and the excavation site was backfilled. The investigation of the underlying cause of the leak was performed and the source of the leak was identified as a weld seam. This piece of pipe was cut out and replaced.
Detailed record list
Report Received Date
2010-09-08 00:00:00
Iyear
2010
Report Number
20100195
Supplemental Number
31607
Report Type
Supplemental Final
Operator Id
Name
Bp Pipeline (North America) Inc.
Operator Street Address
30 S. Wacker Drive
Operator City Name
Chicago
Operator State Abbreviation
IL
Operator Postal Code
60606
Local Datetime
2010-08-12 17:00:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Propylene
Unintentional Release Bbls
3
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2010-08-12 17:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Repair Was Performed With Pipeline In Operation
On Site Datetime
2010-08-12 17:30:00
Nrc Rpt Datetime
2010-08-13 16:48:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Mont Belview-Bayport 191 Chemical Grade Propylene
Segment Name
Trrc Segment Id 552401
Onshore State Abbreviation
Tx
Onshore Postal Code
77571
Onshore City Name
Laporte
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
19.34
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Weld, Including Heat-Affected Zone
Pipe Diameter
6
Pipe Wall Thickness
0.188
Pipe Smys
52000
Pipe Specification
5lx-X52
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Weld Subtype
Pipe Girth Weld
Installation Year
1976
Manufactured Year
1976
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
25600
Est Cost Prop Damage
220000
Est Cost Emergency
50000
Est Cost Environmental
0
Est Cost Other
0
Prpty
295600
Accident Psig
585
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
34320
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
It was a pinhole leak below leak detection threshold.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind
Yes
Failure Type
Design-, Construction-, Installation-, Or Fabrication-Related
Other Factor
Yes
Other Factor Details
Unknown At This Time
Pwf Additional Other Ind
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2007
Geometry Recent Year
2007
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
M*** P* B*****
Preparer Title
Compliance Coordinator
Preparer Email
B*******@b*.com
Preparer Telephone
3377355303
Preparer Fax
3377355492
Prepared Date
2019-02-04 00:00:00
Authorizer Name
M*** P* B*****
Authorizer Telephone
3377355303
Authorizer Title
Compliance Coordinator
Authorizer Email
B*******@b*.com
Narrative
On 8-12-10, during the period between 1645 hrs and 1700 hrs, bp personnel responded to a 3rd party notification of hydrocarbon odors on/near bp's right of way, laporte, texas. Following initial assessment of the potential release site, bp generated an emergency one call, cleared the one-calls and began excavation on the bp-operated propylene pipeline at approximately 1930 hrs. The excavation site was continuously monitored for safe working atmospheric conditions. At approximately 2130 hrs the excavation was completed and the source was confirmed as bp's propylene line. At approximately 2245 hrs the leak was repaired with the installation of a plidco clamp. On 8-13-10 the pipeline was inspected and recoated and the excavation site was backfilled. The investigation of the underlying cause of the leak was performed and the source of the leak was identified as a weld seam. This piece of pipe was cut out and replaced.
Report Received Date 2010-09-08 00:00:00
Iyear 2010
Report Number 20100195
Supplemental Number 31607
Report Type Supplemental Final
Operator Id 31189 PHMSA Enforcement
Name Bp Pipeline (North America) Inc.
Operator Street Address 30 S. Wacker Drive
Operator City Name Chicago
Operator State Abbreviation IL
Operator Postal Code 60606
Local Datetime 2010-08-12 17:00:00
Location Latitude 29.66904 Google Maps OpenStreetMap
Location Longitude -95.05733 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Propylene
Unintentional Release Bbls 3
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2010-08-12 17:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Repair Was Performed With Pipeline In Operation
On Site Datetime 2010-08-12 17:30:00
Nrc Rpt Datetime 2010-08-13 16:48:00
Nrc Rpt Num 950871 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Mont Belview-Bayport 191 Chemical Grade Propylene
Segment Name Trrc Segment Id 552401
Onshore State Abbreviation Tx
Onshore Postal Code 77571
Onshore City Name Laporte
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name 19.34
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48
Crossing No
Pipe Facility Type Intrastate
Item Involved Weld, Including Heat-Affected Zone
Pipe Diameter 6
Pipe Wall Thickness 0.188
Pipe Smys 52000
Pipe Specification 5lx-X52
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Weld Subtype Pipe Girth Weld
Installation Year 1976
Manufactured Year 1976
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 25600
Est Cost Prop Damage 220000
Est Cost Emergency 50000
Est Cost Environmental 0
Est Cost Other 0
Prpty 295600
Accident Psig 585
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 34320
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details It was a pinhole leak below leak detection threshold.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind Yes
Failure Type Design-, Construction-, Installation-, Or Fabrication-Related
Other Factor Yes
Other Factor Details Unknown At This Time
Pwf Additional Other Ind Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2007
Geometry Recent Year 2007
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name M*** P* B*****
Preparer Title Compliance Coordinator
Preparer Email B*******@b*.com
Preparer Telephone 3377355303
Preparer Fax 3377355492
Prepared Date 2019-02-04 00:00:00
Authorizer Name M*** P* B*****
Authorizer Telephone 3377355303
Authorizer Title Compliance Coordinator
Authorizer Email B*******@b*.com
Narrative On 8-12-10, during the period between 1645 hrs and 1700 hrs, bp personnel responded to a 3rd party notification of hydrocarbon odors on/near bp's right of way, laporte, texas. Following initial assessment of the potential release site, bp generated an emergency one call, cleared the one-calls and began excavation on the bp-operated propylene pipeline at approximately 1930 hrs. The excavation site was continuously monitored for safe working atmospheric conditions. At approximately 2130 hrs the excavation was completed and the source was confirmed as bp's propylene line. At approximately 2245 hrs the leak was repaired with the installation of a plidco clamp. On 8-13-10 the pipeline was inspected and recoated and the excavation site was backfilled. The investigation of the underlying cause of the leak was performed and the source of the leak was identified as a weld seam. This piece of pipe was cut out and replaced.

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