HL incident on 2010-07-28 — TX

Operator
Enbridge Energy, Limited Partnership
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
Incident datetime
2010-07-28 07:45
Report number
Location
TX
Narrative
Enbridge field laborers working along the right-of-way reported seeing evidence of oil on the ground around a mainline valve at mp-958.33, which is located north of hwy 2 on the east side of cass lake. The laborers contacted their supervisor who confirmed the release and mobilized enbridge response. Lines 1 and 2 in this route were shut down and valves on either side of the location isolated the section as a precaution. The pipeline maintenance supervisor, who responded to the site, confirmed the valve leak on line 1 and estimated a small amount of oil had been released on the ground around the valve. Enbridge maintenance personnel excavated, by hand, the soil around the site, evaluated the valve condition and confirmed that the valve stem packing was leaking. Enbridge maintenance personnel were able to make on site repairs to the valve stem packing. Estimated volume released was 10 gallons. Once the packing was repaired, the line was restarted at 17:45 pm local time. All affected soil has been removed and disposed at an appropriate off-site facility. The incident was reported to the mn duty officer and the national response center. A representative from mnops visited to inspect the site.
Detailed record list
Report Received Date
2010-08-27 00:00:00
Iyear
2010
Report Number
20100184
Supplemental Number
15264
Report Type
Original Final
Operator Id
Name
Enbridge Energy, Limited Partnership
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2010-07-28 07:45:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.23
Intentional Release Bbls
0
Recovered Bbls
0.23
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2010-07-28 07:45:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2010-07-28 08:00:00
Restart Datetime
2010-07-28 17:45:00
On Site Datetime
2010-07-28 07:55:00
Nrc Rpt Datetime
2010-07-28 10:37:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Pipe Fac Name
Line 1
Segment Name
Valve At Mp 958.33
Onshore State Abbreviation
Mn
Onshore Postal Code
56633
Onshore City Name
Cass Lake
Onshore County Name
Cass
Designated Location
Milepost/valve Station
Designated Name
958.33
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
6
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Gate
Valve Manufacturer
M & J
Installation Year
1951
Manufactured Year
1951
Material Involved
Material Other Than Carbon Steel
Material Details
Valve Stem Packing
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Emergency
3500
Est Cost Environmental
14852
Prpty
18352
Accident Psig
393
Mop Psig
837
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
171758
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller would not be able to detect or control such a small release of product initiated from a valve stem packing.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind
Yes
Eq Additional Other Details
Stem Nut Seal - Normal Wear.
Preparer Name
T****** P*****
Preparer Title
Compliance Analyst
Preparer Email
T*************@e*******.com
Preparer Telephone
715-394-1468
Preparer Fax
832-325-5477
Prepared Date
2010-08-27 00:00:00
Authorizer Name
D**** H******
Authorizer Telephone
715-394-1540
Authorizer Title
Supervisor Pipeline Safety Compliance
Authorizer Email
D************@e*******.com
Narrative
Enbridge field laborers working along the right-of-way reported seeing evidence of oil on the ground around a mainline valve at mp-958.33, which is located north of hwy 2 on the east side of cass lake. The laborers contacted their supervisor who confirmed the release and mobilized enbridge response. Lines 1 and 2 in this route were shut down and valves on either side of the location isolated the section as a precaution. The pipeline maintenance supervisor, who responded to the site, confirmed the valve leak on line 1 and estimated a small amount of oil had been released on the ground around the valve. Enbridge maintenance personnel excavated, by hand, the soil around the site, evaluated the valve condition and confirmed that the valve stem packing was leaking. Enbridge maintenance personnel were able to make on site repairs to the valve stem packing. Estimated volume released was 10 gallons. Once the packing was repaired, the line was restarted at 17:45 pm local time. All affected soil has been removed and disposed at an appropriate off-site facility. The incident was reported to the mn duty officer and the national response center. A representative from mnops visited to inspect the site.
Report Received Date 2010-08-27 00:00:00
Iyear 2010
Report Number 20100184
Supplemental Number 15264
Report Type Original Final
Operator Id 11169 PHMSA Enforcement
Name Enbridge Energy, Limited Partnership
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2010-07-28 07:45:00
Location Latitude 47.372103 Google Maps OpenStreetMap
Location Longitude -94.57539 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.23
Intentional Release Bbls 0
Recovered Bbls 0.23
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2010-07-28 07:45:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2010-07-28 08:00:00
Restart Datetime 2010-07-28 17:45:00
On Site Datetime 2010-07-28 07:55:00
Nrc Rpt Datetime 2010-07-28 10:37:00
Nrc Rpt Num 949152 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Pipe Fac Name Line 1
Segment Name Valve At Mp 958.33
Onshore State Abbreviation Mn
Onshore Postal Code 56633
Onshore City Name Cass Lake
Onshore County Name Cass
Designated Location Milepost/valve Station
Designated Name 958.33
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 6
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Gate
Valve Manufacturer M & J
Installation Year 1951
Manufactured Year 1951
Material Involved Material Other Than Carbon Steel
Material Details Valve Stem Packing
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Emergency 3500
Est Cost Environmental 14852
Prpty 18352
Accident Psig 393
Mop Psig 837
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 171758
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller would not be able to detect or control such a small release of product initiated from a valve stem packing.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind Yes
Eq Additional Other Details Stem Nut Seal - Normal Wear.
Preparer Name T****** P*****
Preparer Title Compliance Analyst
Preparer Email T*************@e*******.com
Preparer Telephone 715-394-1468
Preparer Fax 832-325-5477
Prepared Date 2010-08-27 00:00:00
Authorizer Name D**** H******
Authorizer Telephone 715-394-1540
Authorizer Title Supervisor Pipeline Safety Compliance
Authorizer Email D************@e*******.com
Narrative Enbridge field laborers working along the right-of-way reported seeing evidence of oil on the ground around a mainline valve at mp-958.33, which is located north of hwy 2 on the east side of cass lake. The laborers contacted their supervisor who confirmed the release and mobilized enbridge response. Lines 1 and 2 in this route were shut down and valves on either side of the location isolated the section as a precaution. The pipeline maintenance supervisor, who responded to the site, confirmed the valve leak on line 1 and estimated a small amount of oil had been released on the ground around the valve. Enbridge maintenance personnel excavated, by hand, the soil around the site, evaluated the valve condition and confirmed that the valve stem packing was leaking. Enbridge maintenance personnel were able to make on site repairs to the valve stem packing. Estimated volume released was 10 gallons. Once the packing was repaired, the line was restarted at 17:45 pm local time. All affected soil has been removed and disposed at an appropriate off-site facility. The incident was reported to the mn duty officer and the national response center. A representative from mnops visited to inspect the site.

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