HL incident on 2010-07-19 — TX

Operator
Sfpp, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$400
Incident datetime
2010-07-19 20:44
Report number
Location
TX
Narrative
A release occurred when the poly diaphragm failed on a low suction pressure shut down switch. This allowed product to flow out of the switch housing and onto the soil. At the time of the failure, the operator was gauging a tank for a product switch. When returning to the control room, he noticed the release and immediately isolated the switch, stopping the release. Ls 64 was promptly shut down and notifications began. The switch was replaced with a model containing a stainless diaphragm. * note: part c ' additional facility information (4) ' estimated year of installation
Detailed record list
Report Received Date
2010-08-16 00:00:00
Iyear
2010
Report Number
20100178
Supplemental Number
17329
Report Type
Supplemental Final
Operator Id
Name
Sfpp, Lp
Operator Street Address
500 Dallas Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2010-07-19 20:44:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.94
Intentional Release Bbls
0
Recovered Bbls
0.94
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2010-07-19 20:44:00
Restart Datetime
2010-07-20 07:21:00
Nrc Rpt Datetime
2010-07-19 21:36:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Rocklin Station
Segment Name
Instation Equip Associated With Ls 64
Onshore State Abbreviation
Ca
Onshore Postal Code
95677
Onshore City Name
Rocklin
Onshore County Name
Placer
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Other
Item Involved Details
Low Suction Pressure Shutdown Switch
Installation Year
1957
Material Involved
Material Other Than Carbon Steel
Material Details
Non-Metallic (Poly) Diaphragm
Release Type
Leak
Leak Type
Other
Leak Type Other
Product Seeped From Cover
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
100
Est Cost Prop Damage
400
Est Cost Emergency
35000
Est Cost Environmental
14000
Est Cost Other
0
Prpty
49500
Accident Psig
110
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak was visually discovered by field operator/controller.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Low Suction Pressure Shutdown Switch
Eq Additional Other Ind
Yes
Eq Additional Other Details
Diaphragm Failure, Not A Historically High-Failure Component
Preparer Name
S**** M*******
Preparer Title
Mgr Ccs Pacific Region
Preparer Email
S*************@k***********.com
Preparer Telephone
909-389-6146
Preparer Fax
303-984-3620
Prepared Date
2013-03-04 00:00:00
Authorizer Name
E***** A* F***
Authorizer Telephone
713-369-9454
Authorizer Title
Dir Ccs
Authorizer Email
B********@k***********.com
Narrative
A release occurred when the poly diaphragm failed on a low suction pressure shut down switch. This allowed product to flow out of the switch housing and onto the soil. At the time of the failure, the operator was gauging a tank for a product switch. When returning to the control room, he noticed the release and immediately isolated the switch, stopping the release. Ls 64 was promptly shut down and notifications began. The switch was replaced with a model containing a stainless diaphragm. * note: part c ' additional facility information (4) ' estimated year of installation
Report Received Date 2010-08-16 00:00:00
Iyear 2010
Report Number 20100178
Supplemental Number 17329
Report Type Supplemental Final
Operator Id 18092 PHMSA Enforcement
Name Sfpp, Lp
Operator Street Address 500 Dallas Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2010-07-19 20:44:00
Location Latitude 38.780525 Google Maps OpenStreetMap
Location Longitude -121.246797 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.94
Intentional Release Bbls 0
Recovered Bbls 0.94
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2010-07-19 20:44:00
Restart Datetime 2010-07-20 07:21:00
Nrc Rpt Datetime 2010-07-19 21:36:00
Nrc Rpt Num 948267 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Rocklin Station
Segment Name Instation Equip Associated With Ls 64
Onshore State Abbreviation Ca
Onshore Postal Code 95677
Onshore City Name Rocklin
Onshore County Name Placer
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Other
Item Involved Details Low Suction Pressure Shutdown Switch
Installation Year 1957
Material Involved Material Other Than Carbon Steel
Material Details Non-Metallic (Poly) Diaphragm
Release Type Leak
Leak Type Other
Leak Type Other Product Seeped From Cover
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
Est Cost Oper Paid 0
Est Cost Gas Released 100
Est Cost Prop Damage 400
Est Cost Emergency 35000
Est Cost Environmental 14000
Est Cost Other 0
Prpty 49500
Accident Psig 110
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Leak was visually discovered by field operator/controller.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details Low Suction Pressure Shutdown Switch
Eq Additional Other Ind Yes
Eq Additional Other Details Diaphragm Failure, Not A Historically High-Failure Component
Preparer Name S**** M*******
Preparer Title Mgr Ccs Pacific Region
Preparer Email S*************@k***********.com
Preparer Telephone 909-389-6146
Preparer Fax 303-984-3620
Prepared Date 2013-03-04 00:00:00
Authorizer Name E***** A* F***
Authorizer Telephone 713-369-9454
Authorizer Title Dir Ccs
Authorizer Email B********@k***********.com
Narrative A release occurred when the poly diaphragm failed on a low suction pressure shut down switch. This allowed product to flow out of the switch housing and onto the soil. At the time of the failure, the operator was gauging a tank for a product switch. When returning to the control room, he noticed the release and immediately isolated the switch, stopping the release. Ls 64 was promptly shut down and notifications began. The switch was replaced with a model containing a stainless diaphragm. * note: part c ' additional facility information (4) ' estimated year of installation

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