Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2010-07-14 — OK
Operator
Oneok Ngl Pipeline Lp
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$0
Incident datetime
2010-07-14 12:30
Report number
Location
OK
Narrative
Employee observed product vapor escaping from flange fitting. Bolts on fittings wer re-tightened which stopped vapor leak.
Detailed record list
Report Received Date
2010-08-10 00:00:00
Iyear
2010
Report Number
20100169
Supplemental Number
17306
Report Type
Supplemental Final
Operator Id
32109
Name
Oneok Ngl Pipeline Lp
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2010-07-14 12:30:00
Location Latitude
35.23317
Location Longitude
-97.60874
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
1.5
Intentional Release Bbls
0.1
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2010-07-14 12:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
No Shut Down Was Needed
On Site Datetime
2010-07-14 12:30:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Newcastle Valve Site
Segment Name
Arbuckle Reroute 10025
Onshore State Abbreviation
Ok
Onshore Postal Code
73065
Onshore County Name
Mcclain
Designated Location
Milepost/valve Station
Designated Name
Valve Ar-1
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Flange Assembly
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Gasket
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
49
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
49
Accident Psig
800
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Additional Installation Ind
Yes
Preparer Name
P**** G**********
Preparer Email
P****************@o****.com
Preparer Telephone
580-395-6238
Preparer Fax
580-395-2933
Prepared Date
2013-03-04 00:00:00
Authorizer Name
N*** J****
Authorizer Telephone
580-395-6304
Authorizer Email
N*********@o****.com
Narrative
Employee observed product vapor escaping from flange fitting. Bolts on fittings wer re-tightened which stopped vapor leak.
| Report Received Date | 2010-08-10 00:00:00 |
|---|---|
| Iyear | 2010 |
| Report Number | 20100169 |
| Supplemental Number | 17306 |
| Report Type | Supplemental Final |
| Operator Id | 32109 PHMSA Enforcement |
| Name | Oneok Ngl Pipeline Lp |
| Operator Street Address | 100 West Fifth Street |
| Operator City Name | Tulsa |
| Operator State Abbreviation | OK |
| Operator Postal Code | 74103 |
| Local Datetime | 2010-07-14 12:30:00 |
| Location Latitude | 35.23317 Google Maps OpenStreetMap |
| Location Longitude | -97.60874 Google Maps OpenStreetMap |
| Commodity Released Type | Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions |
| Commodity Subtype | Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid) |
| Unintentional Release Bbls | 1.5 |
| Intentional Release Bbls | 0.1 |
| Recovered Bbls | 0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Local Operating Personnel, Including Contractors |
| Operator Type | Operator Employee |
| Incident Identified Datetime | 2010-07-14 12:30:00 |
| System Part Involved | Onshore Pipeline, Including Valve Sites |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | No Shut Down Was Needed |
| On Site Datetime | 2010-07-14 12:30:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Newcastle Valve Site |
| Segment Name | Arbuckle Reroute 10025 |
| Onshore State Abbreviation | Ok |
| Onshore Postal Code | 73065 |
| Onshore County Name | Mcclain |
| Designated Location | Milepost/valve Station |
| Designated Name | Valve Ar-1 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
| Crossing | No |
| Pipe Facility Type | Intrastate |
| Item Involved | Flange Assembly |
| Material Involved | Carbon Steel |
| Release Type | Leak |
| Leak Type | Other |
| Leak Type Other | Gasket |
| Wildlife Impact Ind | No |
| Soil Contamination | No |
| Long Term Assessment | No |
| Remediation Ind | No |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| Other Pop Ind | Yes |
| Other Pop Yes No | Yes |
| Usa Ecological Ind | Yes |
| Usa Ecological Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 49 |
| Est Cost Prop Damage | 0 |
| Est Cost Emergency | 0 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 49 |
| Accident Psig | 800 |
| Mop Psig | 1440 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Internal Inspection Ind | Yes |
| Operation Complications Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | No |
| Cpm In Place Ind | No |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Non-Threaded Connection Failure |
| Eq Failure Type | Non-Threaded Connection Failure |
| Other Non Threaded Ind | Gasket |
| Additional Installation Ind | Yes |
| Preparer Name | P**** G********** |
| Preparer Email | P****************@o****.com |
| Preparer Telephone | 580-395-6238 |
| Preparer Fax | 580-395-2933 |
| Prepared Date | 2013-03-04 00:00:00 |
| Authorizer Name | N*** J**** |
| Authorizer Telephone | 580-395-6304 |
| Authorizer Email | N*********@o****.com |
| Narrative | Employee observed product vapor escaping from flange fitting. Bolts on fittings wer re-tightened which stopped vapor leak. |
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