HL incident on 2010-06-30 — OK

Operator
Magellan Pipeline Company, Lp
Cause
Corrosion Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$6,000
Incident datetime
2010-06-30 05:00
Report number
Location
OK
Narrative
At 04:58 on june 30 the magellan pipeline company, l.P. Operations control center in tulsa, ok received a call indicating the presence of a strong gasoline odor from a storm sewer adjacent to the subject pipeline. The line was immediately shut down and local magellan personnel called out to investigate, resulting in discovering this release. Repair was made using a pressure-containing full encirclement sleeve, and impacted soil was removed and replaced with clean soil. This updated supplemental-final report is being filed at the request of PHMSA central region. The earliest date and time that magellan became aware of the release was at 04:58 on june 30, 2010 when the omaha fire department called the magellan operations control center as indicated above, at which time magellan instituted its code red procedure, immediately shutting down the line. Magellan has not been able to establish with certainty a time when the release may have occurred earlier than 04:58 june 30, 2010. The omaha fire department flushed the storm sewer system with water, causing some product to impact the water in the city's storm water detention ponds. Magellan does not know the extent of the impact and wishes to stress that the water impact listed in part d #4 and #5 is largely thought to be the result of flushing the sewer systems. Magellan conducted water impact analysis of the detention ponds and treated the water as necessary to ensure the quality of the water released from the detention ponds.
Detailed record list
Report Received Date
2010-07-28 00:00:00
Iyear
2010
Report Number
20100158
Supplemental Number
21757
Report Type
Supplemental Final
Operator Id
Name
Magellan Pipeline Company, Lp
Operator Street Address
One Williams Center, Mail Drop 28
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74172
Local Datetime
2010-06-30 04:58:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
184.14
Intentional Release Bbls
0
Recovered Bbls
148
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Emergency Responder
Incident Identified Datetime
2010-06-30 05:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2010-06-30 05:00:00
Restart Datetime
2010-07-02 17:15:00
On Site Datetime
2010-06-30 06:10:00
Nrc Rpt Datetime
2010-06-30 06:17:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
34
Pipe Fac Name
#1-8" Irvington To Omaha Line
Segment Name
#6230
Onshore State Abbreviation
Ne
Onshore Postal Code
68112-3401
Onshore City Name
Omaha
Onshore County Name
Douglas
Designated Location
Survey Station No.
Designated Name
417+52
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8
Pipe Wall Thickness
0.203
Pipe Smys
35000
Pipe Specification
Api 5l Grade B
Pipe Seam Type
Seamless
Pipe Manufacturer
National Tube
Pipe Coating Type
Coal Tar
Installation Year
1946
Manufactured Year
1946
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
0.1
Rel Water Name
Storm Water Retention Basin
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
35000
Est Cost Gas Released
3100
Est Cost Prop Damage
6000
Est Cost Emergency
620000
Est Cost Environmental
130000
Est Cost Other
12994
Est Cost Other Details
Damages, Lodging And Food For Evacuees
Prpty
807094
Accident Psig
63
Mop Psig
1080
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
30057
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Galvanic Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
1946
Shielding Evident
Yes
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Cp Annual Survey Year
2009
Prior Damage
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Axial Recent Year
2010
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
1990
Hydrtst Most Rcnt Pressure
1496
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
K****** L* L*******
Preparer Title
Senior Compliance Coordinator
Preparer Email
K***************@m*********.com
Preparer Telephone
918-574-7315
Preparer Fax
918-574-7246
Prepared Date
2016-10-13 00:00:00
Authorizer Name
K****** L* L*******
Authorizer Telephone
918-574-7315
Authorizer Title
Senior Compliance Coordinator
Authorizer Email
K***************@m*********.com
Narrative
At 04:58 on june 30 the magellan pipeline company, l.P. Operations control center in tulsa, ok received a call indicating the presence of a strong gasoline odor from a storm sewer adjacent to the subject pipeline. The line was immediately shut down and local magellan personnel called out to investigate, resulting in discovering this release. Repair was made using a pressure-containing full encirclement sleeve, and impacted soil was removed and replaced with clean soil. This updated supplemental-final report is being filed at the request of PHMSA central region. The earliest date and time that magellan became aware of the release was at 04:58 on june 30, 2010 when the omaha fire department called the magellan operations control center as indicated above, at which time magellan instituted its code red procedure, immediately shutting down the line. Magellan has not been able to establish with certainty a time when the release may have occurred earlier than 04:58 june 30, 2010. The omaha fire department flushed the storm sewer system with water, causing some product to impact the water in the city's storm water detention ponds. Magellan does not know the extent of the impact and wishes to stress that the water impact listed in part d #4 and #5 is largely thought to be the result of flushing the sewer systems. Magellan conducted water impact analysis of the detention ponds and treated the water as necessary to ensure the quality of the water released from the detention ponds.
Report Received Date 2010-07-28 00:00:00
Iyear 2010
Report Number 20100158
Supplemental Number 21757
Report Type Supplemental Final
Operator Id 22610 PHMSA Enforcement
Name Magellan Pipeline Company, Lp
Operator Street Address One Williams Center, Mail Drop 28
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74172
Local Datetime 2010-06-30 04:58:00
Location Latitude 41.31825 Google Maps OpenStreetMap
Location Longitude -95.93717 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 184.14
Intentional Release Bbls 0
Recovered Bbls 148
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Emergency Responder
Incident Identified Datetime 2010-06-30 05:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2010-06-30 05:00:00
Restart Datetime 2010-07-02 17:15:00
On Site Datetime 2010-06-30 06:10:00
Nrc Rpt Datetime 2010-06-30 06:17:00
Nrc Rpt Num 946008 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 34
Pipe Fac Name #1-8" Irvington To Omaha Line
Segment Name #6230
Onshore State Abbreviation Ne
Onshore Postal Code 68112-3401
Onshore City Name Omaha
Onshore County Name Douglas
Designated Location Survey Station No.
Designated Name 417+52
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 8
Pipe Wall Thickness 0.203
Pipe Smys 35000
Pipe Specification Api 5l Grade B
Pipe Seam Type Seamless
Pipe Manufacturer National Tube
Pipe Coating Type Coal Tar
Installation Year 1946
Manufactured Year 1946
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Amount Released 0.1
Rel Water Name Storm Water Retention Basin
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 35000
Est Cost Gas Released 3100
Est Cost Prop Damage 6000
Est Cost Emergency 620000
Est Cost Environmental 130000
Est Cost Other 12994
Est Cost Other Details Damages, Lodging And Food For Evacuees
Prpty 807094
Accident Psig 63
Mop Psig 1080
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 30057
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 1
Num Employees Failed 0
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Galvanic Corrosion Ind Yes
Field Exam Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year 1946
Shielding Evident Yes
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Cp Annual Survey Year 2009
Prior Damage Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Axial Recent Year 2010
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 1990
Hydrtst Most Rcnt Pressure 1496
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name K****** L* L*******
Preparer Title Senior Compliance Coordinator
Preparer Email K***************@m*********.com
Preparer Telephone 918-574-7315
Preparer Fax 918-574-7246
Prepared Date 2016-10-13 00:00:00
Authorizer Name K****** L* L*******
Authorizer Telephone 918-574-7315
Authorizer Title Senior Compliance Coordinator
Authorizer Email K***************@m*********.com
Narrative At 04:58 on june 30 the magellan pipeline company, l.P. Operations control center in tulsa, ok received a call indicating the presence of a strong gasoline odor from a storm sewer adjacent to the subject pipeline. The line was immediately shut down and local magellan personnel called out to investigate, resulting in discovering this release. Repair was made using a pressure-containing full encirclement sleeve, and impacted soil was removed and replaced with clean soil. This updated supplemental-final report is being filed at the request of PHMSA central region. The earliest date and time that magellan became aware of the release was at 04:58 on june 30, 2010 when the omaha fire department called the magellan operations control center as indicated above, at which time magellan instituted its code red procedure, immediately shutting down the line. Magellan has not been able to establish with certainty a time when the release may have occurred earlier than 04:58 june 30, 2010. The omaha fire department flushed the storm sewer system with water, causing some product to impact the water in the city's storm water detention ponds. Magellan does not know the extent of the impact and wishes to stress that the water impact listed in part d #4 and #5 is largely thought to be the result of flushing the sewer systems. Magellan conducted water impact analysis of the detention ponds and treated the water as necessary to ensure the quality of the water released from the detention ponds.

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