Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2010-06-25 — TX
Operator
West Texas Gulf Pipeline Co
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$20,300
Incident datetime
2010-06-25 09:55
Report number
Location
TX
Narrative
Internal corrosion on 24" suction/fill line to tank #4 resulting in a 2 barrel release of crude oil. Re-submitted on 3/19/2013 to include part e5f per PHMSA request.
Detailed record list
Report Received Date
2010-07-23 00:00:00
Iyear
2010
Report Number
20100155
Supplemental Number
17581
Report Type
Supplemental Final
Operator Id
22442
Name
West Texas Gulf Pipeline Co
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2010-06-25 09:55:00
Location Latitude
32.53275
Location Longitude
-100.82947
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2010-06-25 09:55:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Suction Fill Line #4-24" Line To Tank 4 Shut Down/isolated
On Site Datetime
2010-06-25 09:55:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Colorado City Station
Onshore State Abbreviation
Tx
Onshore Postal Code
79526
Onshore City Name
Hermleigh
Onshore County Name
Scurry
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Release Type
Leak
Leak Type
Pinhole
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
160
Est Cost Prop Damage
20300
Est Cost Emergency
1952
Est Cost Environmental
0
Est Cost Other
0
Prpty
22412
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Preparer Name
T*** G* N*******
Preparer Title
Dot Compliance Specialist
Preparer Email
T*********@s**************.com
Preparer Telephone
281-637-6576
Preparer Fax
281-637-6425
Prepared Date
2013-03-19 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Dot Compliance Specialist
Authorizer Email
T*********@s**************.com
Narrative
Internal corrosion on 24" suction/fill line to tank #4 resulting in a 2 barrel release of crude oil. Re-submitted on 3/19/2013 to include part e5f per PHMSA request.
| Report Received Date | 2010-07-23 00:00:00 |
|---|---|
| Iyear | 2010 |
| Report Number | 20100155 |
| Supplemental Number | 17581 |
| Report Type | Supplemental Final |
| Operator Id | 22442 PHMSA Enforcement |
| Name | West Texas Gulf Pipeline Co |
| Operator Street Address | 1300 Main Street |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2010-06-25 09:55:00 |
| Location Latitude | 32.53275 Google Maps OpenStreetMap |
| Location Longitude | -100.82947 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 2 |
| Intentional Release Bbls | 0 |
| Recovered Bbls | 0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2010-06-25 09:55:00 |
| System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | Suction Fill Line #4-24" Line To Tank 4 Shut Down/isolated |
| On Site Datetime | 2010-06-25 09:55:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Colorado City Station |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 79526 |
| Onshore City Name | Hermleigh |
| Onshore County Name | Scurry |
| Designated Location | Milepost/valve Station |
| Designated Name | 0 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
| Pipe Facility Type | Interstate |
| Item Involved | Pipe |
| Pipe Type | Pipe Body |
| Release Type | Leak |
| Leak Type | Pinhole |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 160 |
| Est Cost Prop Damage | 20300 |
| Est Cost Emergency | 1952 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 22412 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Corrosion Failure |
| Cause Details | Internal Corrosion |
| Internal External | Internal Corrosion |
| Preparer Name | T*** G* N******* |
| Preparer Title | Dot Compliance Specialist |
| Preparer Email | T*********@s**************.com |
| Preparer Telephone | 281-637-6576 |
| Preparer Fax | 281-637-6425 |
| Prepared Date | 2013-03-19 00:00:00 |
| Authorizer Name | T*** G* N******* |
| Authorizer Telephone | 281-637-6576 |
| Authorizer Title | Dot Compliance Specialist |
| Authorizer Email | T*********@s**************.com |
| Narrative | Internal corrosion on 24" suction/fill line to tank #4 resulting in a 2 barrel release of crude oil. Re-submitted on 3/19/2013 to include part e5f per PHMSA request. |
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