HL incident on 2010-07-17 — OH

Operator
Marathon Pipe Line Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$7,215
Incident datetime
2010-07-17 13:15
Report number
Location
OH
Narrative
At 10:37 the operations center (oc) received a call from a landowner regarding a vapor and smell of product at catlin station. All systems in parke county, indiana were shut down. The oc notified the martinsville area and personnel were dispatched to the site. Upon arrival, a relase of diesel fuel was found at the station. The release was limited to within the station fence and did not leave mpl property. The source of the release was found to be the tubing run around the control valve. The tubing had cracked at the fitting upstream of the control valve. The free-standing diesel fuel was cleaned up using diapers and a vacuum truck. Absorbent boom was placed around the perimeter of the area. The contaminated rock was removed. The tubing run was replaced and pressure-tested. The system and station were restarted at 16:14 without incident. The volume released is estimated to be 25 gallons per calculations perfomed by mpl es&r using observations provided by on-site personnel. Mpl hr and operations supervisor determined drug testing of field technicians not necessary due to the fact that tubing work had not been performed at the station within the last 32 hours.
Detailed record list
Report Received Date
2010-07-22 00:00:00
Iyear
2010
Report Number
20100153
Supplemental Number
17961
Report Type
Supplemental Final
Operator Id
Name
Marathon Pipe Line Llc
Operator Street Address
539 South Main Street
Operator City Name
Findlay
Operator State Abbreviation
OH
Operator Postal Code
45840
Local Datetime
2010-07-17 11:37:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
0.6
Intentional Release Bbls
0
Recovered Bbls
0.6
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2010-07-17 13:15:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2010-07-17 11:46:00
Restart Datetime
2010-07-17 17:14:00
On Site Datetime
2010-07-17 13:15:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Wood River To Clermont 10" Products
Segment Name
Catlin-Jamestown 10"
Onshore State Abbreviation
In
Onshore Postal Code
47872
Onshore City Name
Rockville
Onshore County Name
Parke
Designated Location
Milepost/valve Station
Designated Name
Catlin Stn
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Pipe Facility Type
Interstate
Item Involved
Tubing
Release Type
Other
Release Type Details
The Tubing Had Cracked At The Fitting Upstream Of The Control Valve.
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
75
Est Cost Prop Damage
7215
Est Cost Emergency
14114
Est Cost Environmental
0
Est Cost Other
0
Prpty
21404
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Defective Or Loose Tubing Or Fitting
Eq Failure Type
Defective Or Loose Tubing Or Fitting
Preparer Name
R**** S********
Preparer Title
Hes Professional
Preparer Email
R**********@m****************.com
Preparer Telephone
4194212121
Prepared Date
2013-04-29 00:00:00
Authorizer Name
R****** B*****
Authorizer Telephone
4194212121
Authorizer Title
Regulatory Compliance Supervisor
Authorizer Email
R*******@m****************.com
Narrative
At 10:37 the operations center (oc) received a call from a landowner regarding a vapor and smell of product at catlin station. All systems in parke county, indiana were shut down. The oc notified the martinsville area and personnel were dispatched to the site. Upon arrival, a relase of diesel fuel was found at the station. The release was limited to within the station fence and did not leave mpl property. The source of the release was found to be the tubing run around the control valve. The tubing had cracked at the fitting upstream of the control valve. The free-standing diesel fuel was cleaned up using diapers and a vacuum truck. Absorbent boom was placed around the perimeter of the area. The contaminated rock was removed. The tubing run was replaced and pressure-tested. The system and station were restarted at 16:14 without incident. The volume released is estimated to be 25 gallons per calculations perfomed by mpl es&r using observations provided by on-site personnel. Mpl hr and operations supervisor determined drug testing of field technicians not necessary due to the fact that tubing work had not been performed at the station within the last 32 hours.
Report Received Date 2010-07-22 00:00:00
Iyear 2010
Report Number 20100153
Supplemental Number 17961
Report Type Supplemental Final
Operator Id 32147 PHMSA Enforcement
Name Marathon Pipe Line Llc
Operator Street Address 539 South Main Street
Operator City Name Findlay
Operator State Abbreviation OH
Operator Postal Code 45840
Local Datetime 2010-07-17 11:37:00
Location Latitude 39.68524 Google Maps OpenStreetMap
Location Longitude -87.236533 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 0.6
Intentional Release Bbls 0
Recovered Bbls 0.6
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2010-07-17 13:15:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2010-07-17 11:46:00
Restart Datetime 2010-07-17 17:14:00
On Site Datetime 2010-07-17 13:15:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Wood River To Clermont 10" Products
Segment Name Catlin-Jamestown 10"
Onshore State Abbreviation In
Onshore Postal Code 47872
Onshore City Name Rockville
Onshore County Name Parke
Designated Location Milepost/valve Station
Designated Name Catlin Stn
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Pipe Facility Type Interstate
Item Involved Tubing
Release Type Other
Release Type Details The Tubing Had Cracked At The Fitting Upstream Of The Control Valve.
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 75
Est Cost Prop Damage 7215
Est Cost Emergency 14114
Est Cost Environmental 0
Est Cost Other 0
Prpty 21404
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Defective Or Loose Tubing Or Fitting
Eq Failure Type Defective Or Loose Tubing Or Fitting
Preparer Name R**** S********
Preparer Title Hes Professional
Preparer Email R**********@m****************.com
Preparer Telephone 4194212121
Prepared Date 2013-04-29 00:00:00
Authorizer Name R****** B*****
Authorizer Telephone 4194212121
Authorizer Title Regulatory Compliance Supervisor
Authorizer Email R*******@m****************.com
Narrative At 10:37 the operations center (oc) received a call from a landowner regarding a vapor and smell of product at catlin station. All systems in parke county, indiana were shut down. The oc notified the martinsville area and personnel were dispatched to the site. Upon arrival, a relase of diesel fuel was found at the station. The release was limited to within the station fence and did not leave mpl property. The source of the release was found to be the tubing run around the control valve. The tubing had cracked at the fitting upstream of the control valve. The free-standing diesel fuel was cleaned up using diapers and a vacuum truck. Absorbent boom was placed around the perimeter of the area. The contaminated rock was removed. The tubing run was replaced and pressure-tested. The system and station were restarted at 16:14 without incident. The volume released is estimated to be 25 gallons per calculations perfomed by mpl es&r using observations provided by on-site personnel. Mpl hr and operations supervisor determined drug testing of field technicians not necessary due to the fact that tubing work had not been performed at the station within the last 32 hours.

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