HL incident on 2010-06-10 — TX

Operator
Sunoco Pipeline L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,500
Incident datetime
2010-06-10 04:30
Report number
Location
TX
Narrative
The pump seal had a crack due to fatigue allowing oil to be released into the pump room concrete containment. Re-submitted on 3/27/2013 to include part e5f per PHMSA request.
Detailed record list
Report Received Date
2010-07-09 00:00:00
Iyear
2010
Report Number
20100144
Supplemental Number
17714
Report Type
Supplemental Final
Operator Id
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2010-06-10 04:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.5
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2010-06-10 04:30:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Shut Down Was Not Needed
On Site Datetime
2010-06-10 08:30:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Douglas Station
Segment Name
Et-10"
Onshore State Abbreviation
Tx
Onshore Postal Code
75943
Onshore City Name
Douglas
Onshore County Name
Nacogdoches
Designated Location
Milepost/valve Station
Designated Name
135
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Pipe Facility Type
Intrastate
Item Involved
Pump
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
36
Est Cost Prop Damage
2500
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
2536
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Eq Additional Other Details
Fatigue
Preparer Name
K****** D**** B***
Preparer Title
Area Dot Compliance Supervisor
Preparer Email
K*****@s**************.com
Preparer Telephone
281-637-6497
Preparer Fax
281-637-6425
Prepared Date
2013-03-27 00:00:00
Authorizer Name
K****** D**** B***
Authorizer Telephone
281-637-6497
Authorizer Title
Area Dot Compliance Supervisor
Authorizer Email
K*****@s**************.com
Narrative
The pump seal had a crack due to fatigue allowing oil to be released into the pump room concrete containment. Re-submitted on 3/27/2013 to include part e5f per PHMSA request.
Report Received Date 2010-07-09 00:00:00
Iyear 2010
Report Number 20100144
Supplemental Number 17714
Report Type Supplemental Final
Operator Id 18718 PHMSA Enforcement
Name Sunoco Pipeline L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2010-06-10 04:30:00
Location Latitude 31.65608 Google Maps OpenStreetMap
Location Longitude -94.84362 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.5
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2010-06-10 04:30:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Shut Down Was Not Needed
On Site Datetime 2010-06-10 08:30:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Douglas Station
Segment Name Et-10"
Onshore State Abbreviation Tx
Onshore Postal Code 75943
Onshore City Name Douglas
Onshore County Name Nacogdoches
Designated Location Milepost/valve Station
Designated Name 135
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Pipe Facility Type Intrastate
Item Involved Pump
Release Type Leak
Leak Type Seal Or Packing
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 36
Est Cost Prop Damage 2500
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 2536
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Eq Additional Other Details Fatigue
Preparer Name K****** D**** B***
Preparer Title Area Dot Compliance Supervisor
Preparer Email K*****@s**************.com
Preparer Telephone 281-637-6497
Preparer Fax 281-637-6425
Prepared Date 2013-03-27 00:00:00
Authorizer Name K****** D**** B***
Authorizer Telephone 281-637-6497
Authorizer Title Area Dot Compliance Supervisor
Authorizer Email K*****@s**************.com
Narrative The pump seal had a crack due to fatigue allowing oil to be released into the pump room concrete containment. Re-submitted on 3/27/2013 to include part e5f per PHMSA request.

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