HL incident on 2010-06-23 — OH

Operator
Marathon Pipe Line Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2010-06-23 12:09
Report number
Location
OH
Narrative
Densitometer pump drilled a hole out the end of the body cavity, and sprayed approximately 4.5 barrels of crude oil into the sample building and out onto the surrounding soil.
Detailed record list
Report Received Date
2010-07-09 00:00:00
Iyear
2010
Report Number
20100143
Supplemental Number
17959
Report Type
Supplemental Final
Operator Id
Name
Marathon Pipe Line Llc
Operator Street Address
539 South Main Street
Operator City Name
Findlay
Operator State Abbreviation
OH
Operator Postal Code
45840
Local Datetime
2010-06-23 12:09:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
4.47
Intentional Release Bbls
0
Recovered Bbls
4.47
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2010-06-23 12:09:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2010-06-23 12:09:00
Restart Datetime
2010-06-23 16:23:00
On Site Datetime
2010-06-23 12:15:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Lima To Canton 12" - 16" Crude
Segment Name
Lima Tank Farm - Kenton 12"
Onshore State Abbreviation
Oh
Onshore Postal Code
45801
Onshore City Name
Lima
Onshore County Name
Allen
Designated Location
Milepost/valve Station
Designated Name
Tank Farm
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Inside A Building
Pipe Facility Type
Intrastate
Item Involved
Pump
Release Type
Mechanical Puncture
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
346
Est Cost Prop Damage
0
Est Cost Emergency
42451
Est Cost Environmental
0
Est Cost Other
0
Prpty
42797
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Preparer Name
R**** S********
Preparer Title
Hes Professional
Preparer Email
R**********@m****************.com
Preparer Telephone
4194212121
Prepared Date
2013-04-29 00:00:00
Authorizer Name
R****** B*****
Authorizer Telephone
4194212121
Authorizer Title
Regulatory Compliance Supervisor
Authorizer Email
R*******@m****************.com
Narrative
Densitometer pump drilled a hole out the end of the body cavity, and sprayed approximately 4.5 barrels of crude oil into the sample building and out onto the surrounding soil.
Report Received Date 2010-07-09 00:00:00
Iyear 2010
Report Number 20100143
Supplemental Number 17959
Report Type Supplemental Final
Operator Id 32147 PHMSA Enforcement
Name Marathon Pipe Line Llc
Operator Street Address 539 South Main Street
Operator City Name Findlay
Operator State Abbreviation OH
Operator Postal Code 45840
Local Datetime 2010-06-23 12:09:00
Location Latitude 40.706418 Google Maps OpenStreetMap
Location Longitude -84.113285 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 4.47
Intentional Release Bbls 0
Recovered Bbls 4.47
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2010-06-23 12:09:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2010-06-23 12:09:00
Restart Datetime 2010-06-23 16:23:00
On Site Datetime 2010-06-23 12:15:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Lima To Canton 12" - 16" Crude
Segment Name Lima Tank Farm - Kenton 12"
Onshore State Abbreviation Oh
Onshore Postal Code 45801
Onshore City Name Lima
Onshore County Name Allen
Designated Location Milepost/valve Station
Designated Name Tank Farm
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Inside A Building
Pipe Facility Type Intrastate
Item Involved Pump
Release Type Mechanical Puncture
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 346
Est Cost Prop Damage 0
Est Cost Emergency 42451
Est Cost Environmental 0
Est Cost Other 0
Prpty 42797
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Preparer Name R**** S********
Preparer Title Hes Professional
Preparer Email R**********@m****************.com
Preparer Telephone 4194212121
Prepared Date 2013-04-29 00:00:00
Authorizer Name R****** B*****
Authorizer Telephone 4194212121
Authorizer Title Regulatory Compliance Supervisor
Authorizer Email R*******@m****************.com
Narrative Densitometer pump drilled a hole out the end of the body cavity, and sprayed approximately 4.5 barrels of crude oil into the sample building and out onto the surrounding soil.

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