Incident details
Operator, cause, commodity and consequences with raw source fields.
GD incident on 2010-09-08 — GA
Operator
Atlanta Gas Light Co
Cause
Locating Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$3,973
Incident datetime
2010-09-08 11:54
Report number
Location
GA, RICHMOND
Narrative
Utility company installing cable tv damaged a 6-inch steel natural gas main by directional boring.
Detailed record list
Occurred At
2010-09-08 11:54:00
Year
2010
Report Received Date
2010-10-01 00:00:00
Iyear
2010.0
Report Number
20100076.0
Supplemental Number
15104.0
Report Type
Original Final
Operator Id
Name
Atlanta Gas Light Co
Operator Street Address
10 Peachtree Place Ne
Operator City Name
Atlanta
Operator State Abbreviation
GA
Operator Postal Code
30309
Local Datetime
2010-09-08 11:54:00
Location Street Address
3529 - 3531 Walton Way Extension
Location City Name
Augusta
Location County Name
Richmond
Location State Abbreviation
GA
Location Postal Code
30909
Location Latitude
33.487142
Location Longitude
-82.072715
Nrc Rpt Datetime
2010-09-10 11:52:00
Nrc Rpt Num
953622
Commodity Released Type
Natural Gas
Unintentional Release
13082.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
300.0
Incident Identified Datetime
2010-09-08 11:54:00
On Site Datetime
2010-09-08 12:23:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
54.0
Crossing
No
Pipe Facility Type
Privately Owned
System Part Involved
Main
Installation Year
1967.0
Pipe Diameter
6.625
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Release Type
Mechanical Puncture
Puncture Axial
3.0
Puncture Circum
4.0
Class Location Type
Class 3 Location
Est Cost Oper Paid
38594.0
Est Cost Prop Damage
3973.0
Est Cost Emergency
8760.0
Est Cost Unintentional Release
65413.0
Prpty
116740.0
Commercial Affected
49.0
Industrial Affected
0.0
Residences Affected
72.0
Accident Psig
277.0
Normal Psig
277.0
Mop Psig
300.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
Yes
Num Contractors Tested
1
Num Contractors Failed
0
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
Notify Cga Dirt
Yes
Public Row Ind
Yes
Public Subtype
City Street
Excavator Type
Utility
Excavator Equipment
Directional Drilling
Work Performed
Cable Tv
One Call Notified Ind
Yes
One Call Ticket Num
8250301737
One Call Center Name
Utility Protection Center
Locator Type
Contract Locator
Visible Marks
No
Service Interruption
Yes
Service Interruption Hours
8.0
Root Cause Category
Locating Issue
Root Cause Type
Facility Not Marked Due To Locator Error
Preparer Name
R**** T* M*******
Preparer Title
Senior Compliance Engineer Regulatory Compliance
Preparer Email
R*******@a***********.com
Preparer Telephone
(404) 584-3733
Preparer Fax
(404) 584-4708
Authorizer Name
R****** R* L***
Authorizer Title
Director Regulatory Compliance
Authorizer Telephone
(404) 584-3552
Authorizer Email
R****@a***********.com
Narrative
Utility company installing cable tv damaged a 6-inch steel natural gas main by directional boring.
| Occurred At | 2010-09-08 11:54:00 |
|---|---|
| Year | 2010 |
| Report Received Date | 2010-10-01 00:00:00 |
| Iyear | 2010.0 |
| Report Number | 20100076.0 |
| Supplemental Number | 15104.0 |
| Report Type | Original Final |
| Operator Id | 792 PHMSA Enforcement |
| Name | Atlanta Gas Light Co |
| Operator Street Address | 10 Peachtree Place Ne |
| Operator City Name | Atlanta |
| Operator State Abbreviation | GA |
| Operator Postal Code | 30309 |
| Local Datetime | 2010-09-08 11:54:00 |
| Location Street Address | 3529 - 3531 Walton Way Extension |
| Location City Name | Augusta |
| Location County Name | Richmond |
| Location State Abbreviation | GA |
| Location Postal Code | 30909 |
| Location Latitude | 33.487142 Google Maps OpenStreetMap |
| Location Longitude | -82.072715 Google Maps OpenStreetMap |
| Nrc Rpt Datetime | 2010-09-10 11:52:00 |
| Nrc Rpt Num | 953622 NRC Report How to search |
| Commodity Released Type | Natural Gas |
| Unintentional Release | 13082.0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 300.0 |
| Incident Identified Datetime | 2010-09-08 11:54:00 |
| On Site Datetime | 2010-09-08 12:23:00 |
| Federal | No |
| Location Type | Public Property |
| Incident Area Type | Underground |
| Incident Area Subtype | Under Pavement |
| Depth Of Cover | 54.0 |
| Crossing | No |
| Pipe Facility Type | Privately Owned |
| System Part Involved | Main |
| Installation Year | 1967.0 |
| Pipe Diameter | 6.625 |
| Pipe Specification | Unknown |
| Pipe Manufacturer | Unknown |
| Material Involved | Steel |
| Steel Seam Type | Other |
| Steel Seam Type Details | Unknown |
| Release Type | Mechanical Puncture |
| Puncture Axial | 3.0 |
| Puncture Circum | 4.0 |
| Class Location Type | Class 3 Location |
| Est Cost Oper Paid | 38594.0 |
| Est Cost Prop Damage | 3973.0 |
| Est Cost Emergency | 8760.0 |
| Est Cost Unintentional Release | 65413.0 |
| Prpty | 116740.0 |
| Commercial Affected | 49.0 |
| Industrial Affected | 0.0 |
| Residences Affected | 72.0 |
| Accident Psig | 277.0 |
| Normal Psig | 277.0 |
| Mop Psig | 300.0 |
| Accident Pressure | Pressure Did Not Exceed Maop |
| Scada In Place Ind | No |
| Accident Identifier | Notification From Third Party That Caused The Incident |
| Investigation Status | No, the facility was not monitored by a controller(s) at the time of the incident |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | Yes |
| Num Contractors Tested | 1 |
| Num Contractors Failed | 0 |
| Cause | Excavation Damage |
| Cause Details | Excavation Damage By Third Party |
| Ex Party Type | Excavation Damage By Third Party |
| Prior Notification Ind | Yes |
| One Call System Ind | Yes |
| Notify Cga Dirt | Yes |
| Public Row Ind | Yes |
| Public Subtype | City Street |
| Excavator Type | Utility |
| Excavator Equipment | Directional Drilling |
| Work Performed | Cable Tv |
| One Call Notified Ind | Yes |
| One Call Ticket Num | 8250301737 |
| One Call Center Name | Utility Protection Center |
| Locator Type | Contract Locator |
| Visible Marks | No |
| Service Interruption | Yes |
| Service Interruption Hours | 8.0 |
| Root Cause Category | Locating Issue |
| Root Cause Type | Facility Not Marked Due To Locator Error |
| Preparer Name | R**** T* M******* |
| Preparer Title | Senior Compliance Engineer Regulatory Compliance |
| Preparer Email | R*******@a***********.com |
| Preparer Telephone | (404) 584-3733 |
| Preparer Fax | (404) 584-4708 |
| Authorizer Name | R****** R* L*** |
| Authorizer Title | Director Regulatory Compliance |
| Authorizer Telephone | (404) 584-3552 |
| Authorizer Email | R****@a***********.com |
| Narrative | Utility company installing cable tv damaged a 6-inch steel natural gas main by directional boring. |
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