GTG incident on 2010-06-23 — NE

Operator
Northern Natural Gas Co
Cause
Incorrect Operation
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$25,335
Incident datetime
2010-06-23 09:28
Report number
Location
NE
Narrative
On june 23, 2010, a landowner, eugene mulligan, called northern natural gas company's operations communication center to report blowing gas to atmosphere at a valve site near where he lived. Northern employees immediately responded. It was determined that it was natural gas blowing from northern's mnm80104-m500d mainline at a valve site at approximate milepost 95.89. Pipeline pressure on the line was 739 psig. The line has an maop of 1,000 psig. A pir of 563 feet was calculated. Local police assisted with barricading off 320th street which passes by the valve site. There was no fire, no explosion and no injuries. As a precaution 5 people were evacuated from residences in the near area. Approximately 13 miles of c line and 6 miles of d line were shut in to enable isolation of the line segment. An attempt was made to draw gas pressure down with compression horsepower @ the farmington compressor station. At 490 psig compression was shut down due to high rod load on units. An emergency 1-call was made and contractor personnel were called to assist with repairs. It was determine that line would be blown down to 50 psig for overnight, one person would man site thru the night. On june 24 the line was blown down to zero pressure. Four farmtap customers were impacted. Excavation was commenced and it was found that there was a significant frost ball. A hot water hydro vac was utilized to remove frost. Investigation indicated that there was a portion of the flange gasket blown out, which allowed gas leakage. The flange was disassembled and a new lamons 30" 600 asme b16 47a, asme b1620, 304ir gasket was installed. The flange bolts were re-installed and retorqued. Additional concrete support blocks were installed and allowed to cure. On june 28th the line was purged and slowly reloaded to operational pressure, leak checked, coated and backfilled. A supplemental final report will be filed when all cost of repairs is calculated. Final cost were calculated and initial costs were changed/updated. On april18,2011 a supplemental final report was filed as PHMSA requested to provide additional information on pipe spec's, part c, item 3 of the report and cost of gas released unintentionally in part d, item 7b. This information has been added to this supplemental final report as requested. Supplemental/final report - this report is being filed as a supplemental/final report to report # 20100039-15215 dated 08/31/2010 as a follow up to discussion with PHMSA representatives. Part a item 7 was changed to match time on the nrc form, the cause of the event was changed from equipment failure to incorrect operations. An analysis of the event indicates that there was adequate, proper support for the piping, no indication of subsidence and although the gasket material was not analyzed due to it's damaged condition, there are two other similar 30-inch valves with the same type of gaskets installed on this piping and neither of those have had any problems or leaks, this is a very good, high quality gasket. The leakage appears to have been between the 6 o'clock and 9 o'clock position only. Northern believes that the root cause of this event is most likely that all of the bolts on the flange were not consistently torqued which led to leakage, which ultimately led to the gasket failure. Northern is issuing a technical bulletin to all employees, inspectors and construction personnel re-emphasizing the importance of proper torqueing and the requirements of engineering standard 7570 when joining of pipe & piping components other than by welding. Should there be an event of this nature in the future every effort will be made to ensure that even though the gasket material may be damaged it will be sent to a laboratory for analysis to determine if the quality of the gasket was or is a factor in the event.
Detailed record list
Report Received Date
2010-07-14 00:00:00
Iyear
2010
Report Number
20100039
Supplemental Number
16807
Report Type
Supplemental Final
Operator Id
Name
Northern Natural Gas Co
Operator Street Address
1111 South 103rd Street
Operator City Name
Omaha
Operator State Abbreviation
NE
Operator Postal Code
68124
Local Datetime
2010-06-23 09:22:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2010-06-23 10:45:00
Commodity Released Type
Natural Gas
Unintentional Release
1000
Intentional Release
17933
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2010-06-24 08:00:00
Restart Datetime
2010-06-25 19:00:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
5
Incident Identified Datetime
2010-06-23 09:28:00
On Site Datetime
2010-06-23 10:05:00
On Off Shore
Onshore
Onshore State Abbreviation
Mn
Onshore Postal Code
55057
Onshore City Name
Northfield
Onshore County Name
Dakota
Designated Location
Milepost
Designated Name
95.89
Pipe Fac Name
30-Inch D Line
Segment Name
Mnm80104
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
84
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
30
Pipe Wall Thickness
0.375
Pipe Smys
75000
Pipe Specification
Api 5l
Pipe Seam Type
Single Saw
Pipe Manufacturer
Berg Steel Pipe Co.
Pipe Coating Type
Epoxy
Installation Year
2009
Manufactured Year
2008
Material Involved
Material Other Than Carbon Steel Or Plastic
Material Details
9000 Series Garlock Flange Gasket
Release Type
Leak
Leak Type
Other
Leak Type Other
Flange Gasket
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
563
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
5295
Est Cost Intentional Release
89665
Est Cost Prop Damage
25335
Est Cost Emergency
10000
Est Cost Other
0
Prpty
130295
Accident Psig
739
Mop Psig
1000
Mop Cfr Section
192.619(A)(2)
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
100320
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Public
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The leak was from an underground manually operated valve's flange gasket. Controllers do not have any remote control of this part of pipelines operation. Leak was not significant enough, when found that it would typically be detected by any change in scada pressures.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Equipment Not Installed Properly
Operation Type
Equipment Not Installed Properly
Related Other Ind
Yes
Operation Related Details
It Appears That Engineering Standard 7570 Joining Of Pipe & Piping Components Other Than By Welding Was Not Adequately And Successfully Followed As All Indications Are That The Flange, In Which The Gasket Failed, Was Not Consistently Torqued On All Bolts Around The Flange.
Category Type
Construction
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
B**** W***
Preparer Title
Sr. Pipeline Safety Specialist
Preparer Email
B*********@n****.com
Preparer Telephone
402-398-7396
Preparer Fax
402-398-7706
Authorizer Name
T***** C******
Authorizer Title
Director Of Pipeline Safety And Integrity
Authorizer Telephone
402-398-7715
Authorizer Email
T*************@n****.com
Narrative
O**************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************@ the farmington compressor station. At 490 psig compression was shut down due to high rod load on units. An emergency 1-call was made and contractor personnel were called to assist with repairs. It was determine that line would be blown down to 50 psig for overnight, one person would man site thru the night. On june 24 the line was blown down to zero pressure. Four farmtap customers were impacted. Excavation was commenced and it was found that there was a significant frost ball. A hot water hydro vac was utilized to remove frost. Investigation indicated that there was a portion of the flange gasket blown out, which allowed gas leakage. The flange was disassembled and a new lamons 30" 600 asme b16 47a, asme b1620, 304ir gasket was installed. The flange bolts were re-installed and retorqued. Additional concrete support blocks were installed and allowed to cure. On june 28th the line was purged and slowly reloaded to operational pressure, leak checked, coated and backfilled. A supplemental final report will be filed when all cost of repairs is calculated. Final cost were calculated and initial costs were changed/updated. On april18,2011 a supplemental final report was filed as PHMSA requested to provide additional information on pipe spec's, part c, item 3 of the report and cost of gas released unintentionally in part d, item 7b. This information has been added to this supplemental final report as requested. Supplemental/final report - this report is being filed as a supplemental/final report to report # 20100039-15215 dated 08/31/2010 as a follow up to discussion with PHMSA representatives. Part a item 7 was changed to match time on the nrc form, the cause of the event was changed from equipment failure to incorrect operations. An analysis of the event indicates that there was adequate, proper support for the piping, no indication of subsidence and although the gasket material was not analyzed due to it's damaged condition, there are two other similar 30-inch valves with the same type of gaskets installed on this piping and neither of those have had any problems or leaks, this is a very good, high quality gasket. The leakage appears to have been between the 6 o'clock and 9 o'clock position only. Northern believes that the root cause of this event is most likely that all of the bolts on the flange were not consistently torqued which led to leakage, which ultimately led to the gasket failure. Northern is issuing a technical bulletin to all employees, inspectors and construction personnel re-emphasizing the importance of proper torqueing and the requirements of engineering standard 7570 when joining of pipe & piping components other than by welding. ********************************************************************************************************************************************************************************************************************************************************************.
Report Received Date 2010-07-14 00:00:00
Iyear 2010
Report Number 20100039
Supplemental Number 16807
Report Type Supplemental Final
Operator Id 13750 PHMSA Enforcement
Name Northern Natural Gas Co
Operator Street Address 1111 South 103rd Street
Operator City Name Omaha
Operator State Abbreviation NE
Operator Postal Code 68124
Local Datetime 2010-06-23 09:22:00
Location Latitude 44.48661 Google Maps OpenStreetMap
Location Longitude -93.22225 Google Maps OpenStreetMap
Nrc Rpt Num 945138 NRC Report How to search
Nrc Rpt Datetime 2010-06-23 10:45:00
Commodity Released Type Natural Gas
Unintentional Release 1000
Intentional Release 17933
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind Yes
Shutdown Datetime 2010-06-24 08:00:00
Restart Datetime 2010-06-25 19:00:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 5
Incident Identified Datetime 2010-06-23 09:28:00
On Site Datetime 2010-06-23 10:05:00
On Off Shore Onshore
Onshore State Abbreviation Mn
Onshore Postal Code 55057
Onshore City Name Northfield
Onshore County Name Dakota
Designated Location Milepost
Designated Name 95.89
Pipe Fac Name 30-Inch D Line
Segment Name Mnm80104
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 84
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 30
Pipe Wall Thickness 0.375
Pipe Smys 75000
Pipe Specification Api 5l
Pipe Seam Type Single Saw
Pipe Manufacturer Berg Steel Pipe Co.
Pipe Coating Type Epoxy
Installation Year 2009
Manufactured Year 2008
Material Involved Material Other Than Carbon Steel Or Plastic
Material Details 9000 Series Garlock Flange Gasket
Release Type Leak
Leak Type Other
Leak Type Other Flange Gasket
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 563
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 5295
Est Cost Intentional Release 89665
Est Cost Prop Damage 25335
Est Cost Emergency 10000
Est Cost Other 0
Prpty 130295
Accident Psig 739
Mop Psig 1000
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 100320
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Notification From Public
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The leak was from an underground manually operated valve's flange gasket. Controllers do not have any remote control of this part of pipelines operation. Leak was not significant enough, when found that it would typically be detected by any change in scada pressures.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Equipment Not Installed Properly
Operation Type Equipment Not Installed Properly
Related Other Ind Yes
Operation Related Details It Appears That Engineering Standard 7570 Joining Of Pipe & Piping Components Other Than By Welding Was Not Adequately And Successfully Followed As All Indications Are That The Flange, In Which The Gasket Failed, Was Not Consistently Torqued On All Bolts Around The Flange.
Category Type Construction
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name B**** W***
Preparer Title Sr. Pipeline Safety Specialist
Preparer Email B*********@n****.com
Preparer Telephone 402-398-7396
Preparer Fax 402-398-7706
Authorizer Name T***** C******
Authorizer Title Director Of Pipeline Safety And Integrity
Authorizer Telephone 402-398-7715
Authorizer Email T*************@n****.com
Narrative O**************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************@ the farmington compressor station. At 490 psig compression was shut down due to high rod load on units. An emergency 1-call was made and contractor personnel were called to assist with repairs. It was determine that line would be blown down to 50 psig for overnight, one person would man site thru the night. On june 24 the line was blown down to zero pressure. Four farmtap customers were impacted. Excavation was commenced and it was found that there was a significant frost ball. A hot water hydro vac was utilized to remove frost. Investigation indicated that there was a portion of the flange gasket blown out, which allowed gas leakage. The flange was disassembled and a new lamons 30" 600 asme b16 47a, asme b1620, 304ir gasket was installed. The flange bolts were re-installed and retorqued. Additional concrete support blocks were installed and allowed to cure. On june 28th the line was purged and slowly reloaded to operational pressure, leak checked, coated and backfilled. A supplemental final report will be filed when all cost of repairs is calculated. Final cost were calculated and initial costs were changed/updated. On april18,2011 a supplemental final report was filed as PHMSA requested to provide additional information on pipe spec's, part c, item 3 of the report and cost of gas released unintentionally in part d, item 7b. This information has been added to this supplemental final report as requested. Supplemental/final report - this report is being filed as a supplemental/final report to report # 20100039-15215 dated 08/31/2010 as a follow up to discussion with PHMSA representatives. Part a item 7 was changed to match time on the nrc form, the cause of the event was changed from equipment failure to incorrect operations. An analysis of the event indicates that there was adequate, proper support for the piping, no indication of subsidence and although the gasket material was not analyzed due to it's damaged condition, there are two other similar 30-inch valves with the same type of gaskets installed on this piping and neither of those have had any problems or leaks, this is a very good, high quality gasket. The leakage appears to have been between the 6 o'clock and 9 o'clock position only. Northern believes that the root cause of this event is most likely that all of the bolts on the flange were not consistently torqued which led to leakage, which ultimately led to the gasket failure. Northern is issuing a technical bulletin to all employees, inspectors and construction personnel re-emphasizing the importance of proper torqueing and the requirements of engineering standard 7570 when joining of pipe & piping components other than by welding. ********************************************************************************************************************************************************************************************************************************************************************.

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